ASN Wikibase Occurrence # 202187
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Date: | Saturday 24 April 1999 |
Time: | 11:38 LT |
Type: | Cessna 177 Cardinal |
Owner/operator: | Paul D. And Marcella Steward |
Registration: | N3270T |
MSN: | 17700570 |
Total airframe hrs: | 2443 hours |
Engine model: | Lycoming O-320-E2D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Greencastle, IN -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Chattanooga, TN |
Destination airport: | Lafayette, IN (KLAF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight made a forced landing after an in-flight loss of power and was substantially damaged during roll out. Prior to the flight, the pilot performed a walkaround and found the airplane's fuel was full. He noticed in-flight the left fuel gauge read about 1/2 and less than 1/2 on the right. He decided to divert. The engine was losing power and he attempted an emergency landing in a wet grass and muddy field. After landing, the right fuel cap was found, out of it's filler neck area, on top of the right wing, and in the locked position. The pilot stated that if he had been notified of the fuel cap malfunction, the accident could have been prevented. A lineman parked and fueled the airplane with the owner before the accident. The lineman said the right wing fuel cap was not engaged in its filler neck area, was held on by its chain, and found in the locked position on top of the wing. The lineman stated the right wing had a blue trail down the back of the wing about 8 to 10 inches wide. The lineman said he told the owner about the cap. The lineman re-installed the right cap in its filler neck area on the wing. The cap was examined after the accident and the self-locking nut on the bottom of the fuel cap could be turned by hand. The cap's dome was found not seated on the bolt. The dome could be moved by hand.
Probable Cause: the pilot operating with known deficiencies in equipment and the fuel cap that disengaged. Factors were the wet grass, and muddy terrain conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI99LA131 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB CHI99LA131
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
26-Nov-2017 12:43 |
ASN Update Bot |
Added |
08-Apr-2024 06:44 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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