Incident Beechcraft A36 VH-WMA,
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ASN Wikibase Occurrence # 210670
 
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Date:Thursday 21 August 1997
Time:17:45
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36
Owner/operator:
Registration: VH-WMA
MSN: E-385
Fatalities:Fatalities: 0 / Occupants:
Aircraft damage: Substantial
Location:Charleville Airport (YBCV), Charleville, QLD -   Australia
Phase: Landing
Nature:Passenger - Non-Scheduled/charter/Air Taxi
Departure airport:YBCV
Destination airport:YTWB
Investigating agency: BASI
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that selection of the landing gear up was followed by a loud noise, which appeared to be associated with the landing gear system. The landing gear in-transit light remained illuminated. The pilot remained in the circuit area and selected the landing gear down. This produced green lights for both main gears but no light for the nose gear. The in-transit light remained illuminated. The pilot then attempted to extend the landing gear manually. However, the manual extension lever was jammed and could not be moved. Observers on the ground advised the pilot that the nose gear was swinging backwards and forwards as the aircraft flew overhead. The pilot then attempted to force the nose gear into position by manoeuvring the aircraft. However, the landing gear indication remained unchanged. The pilot subsequently selected the landing gear up and landed the aircraft with the main gear retracted and the nose gear hanging. Examination of the landing gear revealed that the gearbox end of the rear retract rod end for the nose landing had failed. The failure was caused by fatigue crack growth. There was clear evidence of galling between the spherical ball and the outer race. (Galling is adhesive wear between two contacting surfaces and involves localised welding and transfer of materials from one surface to the other.) Under such conditions, then the ball would have been prevented from moving freely during landing gear operation, subjecting the fitting to abnormal operating loads. Advice from the manufacturer indicated that the rod could have been in the aircraft since its manufacture in 1972.

Accident investigation:
cover
  
Investigating agency: BASI
Report number: 
Status: Investigation completed
Duration:
Download report: Final report

Sources:

https://www.atsb.gov.au/publications/investigation_reports/1997/aair/199702707/
https://www.atsb.gov.au/media/4931054/199702707.pdf

Revision history:

Date/timeContributorUpdates
09-May-2018 08:02 Pineapple Added

Corrections or additions? ... Edit this accident description

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