Accident Diamond DA40 Diamond Star N388MA,
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ASN Wikibase Occurrence # 214953
 
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Date:Saturday 1 September 2018
Time:17:15
Type:Silhouette image of generic DA40 model; specific model in this crash may look slightly different    
Diamond DA40 Diamond Star
Owner/operator:Private
Registration: N388MA
MSN: 40.522
Year of manufacture:2005
Total airframe hrs:1386 hours
Engine model:Lycoming IO-360-M1A
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Maury County, Mount Pleasant, TN -   United States of America
Phase: Landing
Nature:Private
Departure airport:Mount Pleasant, TN (MRC)
Destination airport:Mount Pleasant, TN (MRC)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The private pilot reported that, while on a downwind leg of the airport traffic pattern, he reduced the engine power to prepare for landing; however, the engine lost total power. The pilot then advanced the throttle in an unsuccessful attempt to regain power. He subsequently attempted an engine restart to no avail and, at that time, realized that the airplane would not be able to glide to the runway. The pilot performed a forced landing to a field about 1 mile short of the runway threshold, which resulted in substantial damage to the landing gear and empennage. Postaccident examination of the airplane revealed that sufficient fuel remained in the left fuel tank and that the fuel selector was found positioned to the left fuel tank; sufficient fuel also remained in the right fuel tank. Further examination of the engine, fuel system, and ignition system did not reveal any evidence of preimpact mechanical malfunctions or failures that would have precluded normal operation. Although fuel unporting is possible with the amount of fuel that was available in the left tank, it was unlikely based on the airplane’s attitude around the time of the loss of engine power. Thus, the reason for the loss of engine power could not be determined.


Probable Cause: A total loss of engine power for reasons that could not be determined because postaccident examination of the airplane did not reveal any evidence of preimpact mechanical malfunctions or failures that would have precluded normal operation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA18LA241
Status: Investigation completed
Duration: 1 year and 2 months
Download report: Final report

Sources:

NTSB
FAA register: https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=388MA

https://flightaware.com/photos/view/168017-779b9a024f915ae98220e995ee310c3a7f7c99d4/aircrafttype/DA40

History of this aircraft

Other occurrences involving this aircraft
30 June 2010 N388MA Harbor Aviation LLC 0 Farmingdale, New York sub
Runway excursion

Location

Revision history:

Date/timeContributorUpdates
02-Sep-2018 01:06 Geno Added
27-Nov-2019 07:16 ASN Update Bot Updated [Time, Nature, Departure airport, Destination airport, Source, Narrative, Accident report, ]

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