ASN Wikibase Occurrence # 216016
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Date: | Thursday 4 October 2018 |
Time: | 17:30 LT |
Type: | Cessna 210-5A(205A) |
Owner/operator: | Private |
Registration: | N8495Z |
MSN: | 2050495 |
Year of manufacture: | 1963 |
Total airframe hrs: | 3862 hours |
Engine model: | Continental IO-470S |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | SSW of Hefner-Easley Airport (H68), Wagoner, OK -
United States of America
|
Phase: | Take off |
Nature: | Test |
Departure airport: | Wagoner, OK (H68) |
Destination airport: | Wagoner, OK (H68) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During a post maintenance flight after the airplane's annual inspection, the pilot made about three circuits around the airport area before departing to continue flight maneuvers and performance checks. He started a left turn and then noticed a 'very minor engine mis[fire]." As the pilot continued the turn, the "engine mis[fire]" began to increase and the engine began to shake. The airplane was unable to maintain altitude and was descending about 150-300 ft per minute. Although the pilot made multiple attempts to regain engine power, the engine lost total power. The airplane impacted trees and brush; during the landing sequence, the left and right wings buckled.
Following the accident, an engine run was performed; after running for 13 minutes, the engine lost power. Troubleshooting of the magnetos found that the right magneto was firing erratically. The right magneto was replaced with a known-good magneto and the engine was subsequently successfully test run at full power. More detailed testing of both magnetos revealed that they failed the manufacturer's acceptance test procedures due to excessive point gaps and secondary coil resistance. A review of the engine logbooks revealed the magneto points and condensers were replaced about 18 years and about 230 flight hours before the accident flight. Given the available information, it is likely that maintenance personnel did not perform proper maintenance of the magnetos.
Probable Cause: Maintenance personnel's improper maintenance of the magnetos, which resulted in a loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA19LA006 |
Status: | Investigation completed |
Duration: | 3 years and 5 months |
Download report: | Final report |
|
Sources:
NTSB ERA19LA006
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=8495Z%20 Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2018 03:07 |
Geno |
Added |
05-Oct-2018 03:55 |
Geno |
Updated [Aircraft type] |
05-Oct-2018 15:03 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Source] |
02-Jul-2022 17:35 |
ASN Update Bot |
Updated [Time, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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