ASN Wikibase Occurrence # 217614
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Date: | Monday 29 May 2017 |
Time: | 13:30 |
Type: | Zenair CH 601XL |
Owner/operator: | Private |
Registration: | N167EZ |
MSN: | 4942 |
Year of manufacture: | 2016 |
Total airframe hrs: | 60 hours |
Engine model: | Chevrolet Corvair |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sanford, NC -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Apex, NC (NC11) |
Destination airport: | Apex, NC (NC11) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot, who was the builder of the experimental, amateur-built airplane, reported that the airplane was in cruise flight when the engine experienced a total loss of power. He noted that the right fuel tank was empty and that the fuel selector handle was on the left tank. He attempted a restart; however, this was unsuccessful, and he performed a forced landing in a field. The nose landing gear collapsed during the landing roll, resulting in structural damage to the lower fuselage and engine firewall.
Examination of the wreckage revealed that the fuel tank selector handle was on the left tank but the fuel valve remained on the empty right tank. Further examination of the hardware revealed that a threaded metal rod that the pilot installed to connect the tank selector handle to the fuel valve “twisted like bubble gum” when rotated and would not turn the fuel valve. The pilot, who was the airplane builder, used a thinner rod than specified due to an interference problem. This rod was not part of the airplane kit and was improvised by the pilot. The pilot reported that the handle/valve assembly had operated normally during initial testing.
Probable Cause: The pilot’s selection of a threaded metal rod of insufficient strength to connect the fuel tank selector handle to the fuel valve, which resulted in his inability to switch fuel tanks and a subsequent total loss of engine power due to fuel starvation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA17TA196 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
11-Nov-2018 08:36 |
ASN Update Bot |
Added |
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