ASN Wikibase Occurrence # 218212
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Date: | Saturday 17 November 2018 |
Time: | 11:12 |
Type: | Piper PA-28-180 Cherokee |
Owner/operator: | Private |
Registration: | N111TA |
MSN: | 28-3746 |
Year of manufacture: | 1966 |
Total airframe hrs: | 5400 hours |
Engine model: | Lycoming O-360-A4A |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Little Tobesofkee Creek Ranch Airport (GA86), Barnesville, GA -
United States of America
|
Phase: | Take off |
Nature: | Training |
Departure airport: | Barnesville, GA (GA86) |
Destination airport: | Macon Downtown Airport, GA (MAC/KMAC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor reported that the student pilot was taking off for an instructional flight from an upsloping, 3,000-ft-long turf runway with 7- to 8-knot headwinds. The airspeed reached 65 knots and was increasing at the predesignated decision point, which was about 60% of the runway length. After takeoff, the airplane unexpectedly banked left. The student called out that the flight controls were not responding, and the instructor simultaneously took the controls. Realizing that the airplane would not clear trees at the departure end of the runway, the instructor chose to land the airplane straight ahead and aim it between trees. The airplane touched down about 200 ft before the trees and traveled forward until it struck several of them, which resulted in substantial damage to the airframe.
Postaccident examination of the airframe and engine did not reveal evidence of any preaccident mechanical malfunctions or failures that would have precluded normal operation. Further, flight control continuity was confirmed from the flight control surfaces to the cockpit controls. Given that no mechanical anomalies were found during postaccident examination of the airframe, it is likely that the student failed to maintain airplane control during takeoff and that the flight instructor’s delayed remedial action resulted in the subsequent off-runway landing.
Probable Cause: The student pilot’s failure to maintain airplane control during takeoff and the flight instructor’s delayed remedial action, which resulted in an off-runway landing and subsequent collision with trees.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA19LA052 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N111TA%20 Location
Images:
Photo: FAA
Revision history:
Date/time | Contributor | Updates |
21-Nov-2018 08:25 |
Len |
Added |
21-Nov-2018 15:18 |
Geno |
Updated [Aircraft type, Cn, Location, Departure airport, Source, Damage, Narrative] |
19-Apr-2020 06:59 |
ASN Update Bot |
Updated [Time, Operator, Departure airport, Destination airport, Source, Narrative, Accident report, ] |
19-Apr-2020 07:25 |
harro |
Updated [Destination airport, Source, Narrative, Photo, Accident report, ] |
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