Accident Cessna 150J N60486,
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ASN Wikibase Occurrence # 21827
 
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Date:Friday 4 July 2008
Time:16:00
Type:Silhouette image of generic C150 model; specific model in this crash may look slightly different    
Cessna 150J
Owner/operator:Sky Ads
Registration: N60486
MSN: 15070346
Year of manufacture:1969
Engine model:Lycoming O-360
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Seal Beach, CA -   United States of America
Phase: En route
Nature:Banner and glider towing
Departure airport:Compton, CA (CPM)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that he was towing a banner along the ocean shoreline at an altitude of 500 feet and an airspeed of 40 mph when the engine lost power. He dropped the banner into the water, but was unsuccessful in attempting to restart the engine. The pilot ditched the airplane in the ocean about 100 feet from shore. A Federal Aviation Administration inspector examined the airplane after it was pulled onto the beach. The inspector reported that the right wing sustained structural damage. Additionally, the inspector noted that the airplane had been modified extensively, and one of the modifications included replacement of the original two position (ON/OFF) fuel selector valve with a four position fuel selector valve (BOTH ON/LEFT/RIGHT/OFF). The fuel selector valve was found in the LEFT tank position. The left tank contained about 1 gallon of fuel, and the right tank was full of fuel. The pilot stated that he was aware the airplane had been extensively modified, but was not aware that the fuel selector valve had been changed. He further stated that he had never touched the fuel selector switch, as he thought it was ON or OFF only. The operator reported that the pilot had received training in the airplane that included use of the four position fuel selector valve.


Probable Cause: Fuel starvation due to the pilot's improper fuel management procedures and failure to select a tank containing fuel. Contributing to the accident was the lack of suitable terrain for the forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX08CA215
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
24-Jul-2008 11:33 Fusko Added
21-Dec-2016 19:14 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:16 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:20 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
03-Dec-2017 11:26 ASN Update Bot Updated [Operator, Other fatalities, Nature, Departure airport, Source, Narrative]

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