Gear-up landing Accident Beechcraft 35-C33 N829T,
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ASN Wikibase Occurrence # 218677
 
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Date:Sunday 19 July 2015
Time:10:30
Type:Silhouette image of generic BE33 model; specific model in this crash may look slightly different    
Beechcraft 35-C33
Owner/operator:Private
Registration: N829T
MSN: CD-821
Year of manufacture:1964
Total airframe hrs:3181 hours
Engine model:Continental IO 520 SERIES
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Wilmington, NC -   United States of America
Phase: Landing
Nature:Private
Departure airport:Carolina Beach, NC (03NC)
Destination airport:Wilmington, NC (ILM)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial pilot was conducting a short personal flight. According to the pilot, after takeoff, he began receiving faulty airspeed indications and requested an expedited landing from air traffic control because the airplane “did not feel right.” The pilot reported that he kept the landing gear fully extended. He also reported completing the before landing checklist and stated that, during the touchdown, the landing gear “collapsed.”
Postaccident examination of photographs of the airplane found that the main landing gear was partially extended and that the nose landing gear had collapsed. Postaccident examination of the landing gear system revealed that the main landing gear inner doors were in the open position and had been damaged by contact with the runway surface. Scrubbing was found on the sides of the main tires. The nose landing gear was in its wheel well, and the actuating rod was bent, indicating that the nose gear was not fully locked down when it contacted the pavement. The landing gear system circuit breaker was found tripped, which was likely the result of an electrical overload caused by the landing gear extension being physically impeded. There was no evidence of a preimpact malfunction, and a mechanic was able to manually extend the landing gear. Thus, the evidence was consistent with an attempted landing with the landing gear in transit rather than fully extended.

Probable Cause: The pilot's failure to ensure that the landing gear was in the down and locked position before touchdown, which resulted in a landing with the gear in transit.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA15LA273
Status: Investigation completed
Duration: 3 years and 4 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
28-Nov-2018 14:43 ASN Update Bot Added

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