Accident Air Tractor AT-502B N61267,
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ASN Wikibase Occurrence # 218679
 
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Date:Thursday 27 August 2015
Time:12:00
Type:Silhouette image of generic AT5T model; specific model in this crash may look slightly different    
Air Tractor AT-502B
Owner/operator:Red Willow Aviation Spraying Inc
Registration: N61267
MSN: 502B-0303
Year of manufacture:1995
Engine model:Walter M601E11
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Monroe, NE -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Agricultural
Departure airport:Genoa, NE (97Y)
Destination airport:Genoa, NE (97Y)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial pilot was performing an aerial application flight when the airplane experienced a partial loss of engine power. The engine instruments showed that the engine was operating, but was producing less than idle power. The pilot applied full throttle with no effect. He subsequently turned the airplane into the wind, lowered the flaps, and when he heard corn hitting the bottom of the airplane, pulled the control stick full aft to stall the airplane. The left wing dropped and the airplane turned 90° as it impacted the ground. The engine continued to run until the pilot shut it down and exited the airplane.
An examination of the airplane’s engine, propeller governor, fuel control unit, and fuel pump revealed no anomalies. An engine data recorder showed an exceedance of the N1 upper limit, followed by a decrease in internal turbine temperature, N1, and propeller rpm, consistent with a lower output by the engine.
The data were reviewed by the engine manufacturer, who concluded that the data were consistent with a feathered propeller; however, the reason for the propeller feathering could not be determined based on the available information.


Probable Cause: Loss of propeller thrust for reasons that could not be determined, since examination of the airplane's engine, propeller, and associated accessories revealed no anomalies.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN15LA389
Status: Investigation completed
Duration: 3 years and 3 months
Download report: Final report

Sources:

NTSB

History of this aircraft

Other occurrences involving this aircraft
13 August 2008 N61267 Delta Dusters Inc. 0 Tunica, Mississippi sub

Location

Revision history:

Date/timeContributorUpdates
28-Nov-2018 14:43 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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