ASN Wikibase Occurrence # 219118
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Date: | Thursday 6 December 2018 |
Time: | 12:30 LT |
Type: | Beechcraft A36TC Bonanza |
Owner/operator: | Private |
Registration: | N361TC |
MSN: | EA-139 |
Year of manufacture: | 1980 |
Total airframe hrs: | 2813 hours |
Engine model: | Continental IO-550-B-RA |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Los Banos Municipal Airport (KLSN), Los Banos, CA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | San Jose-Reid-Hillview Airport, CA (RHV/KRHV) |
Destination airport: | Los Banos Municipal Airport, CA (LSN/KLSN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After almost 1 hour of flight, the pilot turned onto the left base leg of the traffic pattern at the destination airport, where he intended to practice takeoffs and landings. During the turn, the engine began to sputter. The pilot turned toward the runway and tried to maintain clearance from trees located on the outside of the airport perimeter fence; however, the propeller and landing gear impacted the fence. The airplane came to rest upright about 5 ft from the runway edge, resulting in substantial damage.
Postaccident examination of the engine and fuel system revealed no anomalies. The fuel selector handle had been removed, but the rod that rotated the valve remained intact and attached to the unit. The fuel selector was disassembled, and the ring was found located between detents. Based on its position, it may have been positioned between the left- and right-wing tip tanks; however, the position of the fuel selector at the time of the loss of engine power could not be determined. The pilot reported that there were 74 gallons of fuel onboard at the time of departure; however, neither the distribution of the fuel nor the fuel onboard at the time of the accident was determined.
The reason for the partial loss of engine power could not be determined based on the available information.
Probable Cause: A partial loss of engine power for reasons that could not be determined based on the available information.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR19LA039 |
Status: | Investigation completed |
Duration: | 3 years and 5 months |
Download report: | Final report |
|
Sources:
NTSB WPR19LA039
https://flightaware.com/live/flight/N361TC FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N361TC%20 Location
Revision history:
Date/time | Contributor | Updates |
07-Dec-2018 03:53 |
Geno |
Added |
02-Jul-2022 14:51 |
ASN Update Bot |
Updated [Time, Other fatalities, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report] |
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