ASN Wikibase Occurrence # 221204
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 27 January 2019 |
Time: | 16:34 |
Type: | Beechcraft A36 Bonanza |
Owner/operator: | Private |
Registration: | N36PS |
MSN: | E-1012 |
Year of manufacture: | 1977 |
Total airframe hrs: | 3300 hours |
Engine model: | Continental |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | SE of Fort Worth Meacham Int’l Airport (KFTW), Fort Worth, TX -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Angel Fire Airport, NM (AXX/KAXX) |
Destination airport: | Arlington Municipal Airport, TX (KGKY) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that before departure, both fuel tanks were 3/4 full and that he maintained fuel balance by switching between the left and right tanks "several times" during the flight. As he approached his destination, he requested and received vectors for a practice instrument approach to a nearby airport but then requested termination of the approach and said he would proceed to his original destination. Shortly after the airplane climbed to 1,500 ft (900 ft above ground level), the engine lost power. The pilot switched the fuel selector "to the other tank" and attempted to restart the engine to no avail. He stated that he did not turn on the electric boost pump (as required in the emergency checklist) and that the airplane was too low to the ground for him to reference the emergency checklist.  He lowered the landing gear but did not lower the flaps for landing. The airplane touched down on soft earth, and the nose gear collapsed, resulting in substantial damage to the nose. An unknown quantity of fuel was drained from the left tank, and the right tank was empty. The fuel that was sumped from the airplane’s left tank appeared to be clear, bright, and free of contaminants. The fuel selector was positioned on the left tank. No mechanical malfunctions or failures were noted with the engine or fuel system that would have precluded normal operations. It is likely the engine lost power due to fuel starvation and the pilot failed to switch fuel tanks before exhausting the fuel in the right tank.
Probable Cause: The pilot's improper fuel management, which resulted in fuel starvation and a loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19TA073 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=36PS Location
Images:
Photo: NTSB
Media:
Revision history:
Date/time | Contributor | Updates |
28-Jan-2019 00:03 |
Geno |
Added |
28-Jan-2019 00:05 |
Geno |
Updated [Source] |
28-Jan-2019 06:27 |
RobertMB |
Updated [Aircraft type] |
28-Jan-2019 08:58 |
Iceman 29 |
Updated [Aircraft type, Registration, Cn, Operator, Source] |
28-Jan-2019 08:59 |
Iceman 29 |
Updated [Aircraft type, Registration, Cn, Operator, Source] |
28-Jan-2019 09:00 |
Iceman 29 |
Updated [Embed code] |
28-Jan-2019 17:32 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Source, Embed code, Narrative] |
17-Sep-2019 08:08 |
harro |
Updated [Registration, Departure airport, Destination airport, Source, Narrative] |
15-Aug-2020 16:00 |
ASN Update Bot |
Updated [Time, Operator, Nature, Departure airport, Destination airport, Source, Narrative, Accident report, ] |
15-Aug-2020 16:23 |
harro |
Updated [Departure airport, Destination airport, Source, Narrative, Photo, Accident report, ] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation