ASN Wikibase Occurrence # 223312
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 17 September 2017 |
Time: | 16:00 |
Type: | Cessna 177B Cardinal |
Owner/operator: | Private |
Registration: | N35170 |
MSN: | 17702245 |
Year of manufacture: | 1975 |
Total airframe hrs: | 2054 hours |
Engine model: | Lycoming O-360-A1F6D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | London, OH -
United States of America
|
Phase: | En route |
Nature: | Training |
Departure airport: | London, OH (UYF) |
Destination airport: | London, OH (UYF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor and the student pilot were in a cruise descent toward the destination airport when the engine experienced a total loss of power. The instructor performed a forced landing to a corn field, during which the airplane sustained substantial damage. The instructor reported that the airplane had 25 gallons of fuel onboard before takeoff and that the duration of the accident flight was 1.3 hours. Due to a recent engine overhaul, the instructor was operating the airplane at a high power setting with the mixture full rich. He noted that, during previous flights, the fuel consumption was about 11 gallons per hour and calculated that the airplane should have burned about 14.3 gallons of fuel during the accident flight. Since the engine was not being operated at normal cruise power settings, fuel burn based on information in the pilot's operating handbook could not be calculated; however, examination of the airplane after the accident revealed no usable fuel remaining in either wing fuel tank, and no breaches of the fuel system. Subsequent testing revealed no fuel leakage and no excessive fuel consumption during ground runs.
Based on the available evidence, it is likely that the engine lost power due to fuel exhaustion; however, whether the pilot overestimated the fuel quantity before departure or underestimated the fuel consumption during the flight could not be determined.
Probable Cause: The flight instructor's inadequate in-flight fuel management, which resulted in a total loss of engine power due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN17LA358 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
22-Mar-2019 19:12 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation