ASN Wikibase Occurrence # 223330
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Date: | Monday 7 May 2018 |
Time: | 15:00 |
Type: | Piper PA-18-150 Super Cub |
Owner/operator: | Private |
Registration: | N2432H |
MSN: | 18-7909184 |
Year of manufacture: | 1979 |
Total airframe hrs: | 5214 hours |
Engine model: | Lycoming O320A2B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Goose Bay, AK -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Anchorage-Lake Hood, AK (LHD/PALH) |
Destination airport: | Goose Bay, AK (Z40) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the student pilot in the tailwheel-equipped airplane, during his initial solo flight in the airport traffic pattern, he performed a go-around because “I did not like my approach.” Following the next approach, he recalled that the airplane encountered a left crosswind gust when the airplane touched down on the gravel runway. He believed that the wind had shifted, and the airplane’s tail was “blown” to the right, and its nose turned to the left. The airplane moved from the crown of the runway onto the down-sloping runway edge, and the tailwheel entered the soft gravel. The right wing tip then struck the ground, and the airplane exited the left side of the runway before it came to rest.
The airplane sustained substantial damage to the right wing spar.
The nearest METAR, located 9 miles south of the accident site, reported that, about the time of the accident, the wind was from 280° at 7 knots. The airplane landed on runway 8. The pilot reported that the wind at the time of the accident was variable at 6 knots, gusting to 10 knots.
The student reported that, “I should have caught that there had been a wind shift between my touch and go and when I ground looped my aircraft. In preparation for landing a final check of the windsock needs to be done, every time. If there is a crosswind, a wing low approach would have helped avoid losing control of the aircraft when I touched down.”
The student reported that there were no mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable Cause: The student pilot’s failure to maintain directional control during landing with a gusting tailwind.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA18CA269 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
22-Mar-2019 20:30 |
ASN Update Bot |
Added |
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