ASN Wikibase Occurrence # 223854
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Date: | Saturday 23 July 2016 |
Time: | 13:25 |
Type: | Cessna 310L |
Owner/operator: | Private |
Registration: | N3261X |
MSN: | 310L0111 |
Year of manufacture: | 1967 |
Total airframe hrs: | 3672 hours |
Engine model: | Continental IO-470 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Linden, NJ -
United States of America
|
Phase: | |
Nature: | Private |
Departure airport: | Linden, NJ (LDJ) |
Destination airport: | Linden, NJ (LDJ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot stated that, following a flight in which he was performing a functional check on all systems, when he configured the airplane for landing, he saw three green landing gear lights, visually confirmed that the nose landing gear was down, and then completed the approach for landing. The pilot reported that, at touchdown, he heard a "noise," and the copilot reported hearing a "bang" before the airplane's tail dropped to the runway. During the landing rollout, the copilot attempted to "feather the engines" but was only able to feather the right propeller. The airplane then departed the right side of the runway and settled in grass.
Upon recovery, the nose landing gear were found down and locked, but the main landing gear (MLG) were partially collapsed and would not lock when the airplane was lifted and the gear moved by hand. Examination of the MLG revealed that the landing gear actuator had been driven beyond the down limit switch and that its travel was stopped by the internal stop pin in the actuator. When the landing gear actuator was driven beyond the down limit and toward the internal stop pin, the MLG was released from its down-and-locked position, which allowed it to partially retract before landing. The wreckage was disposed of before a more detailed examination could be performed, and the reason for the overtravel of the MLG actuator could not be determined.
Probable Cause: The overtravel of the main landing gear (MLG) actuator, which resulted in the MLG partially collapsing upon landing. The reasons for the overtravel of the MLG actuator could not be determined due to the unavailability of the wreckage.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA16LA271 |
Status: | Investigation completed |
Duration: | 2 years and 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
10-Apr-2019 12:35 |
ASN Update Bot |
Added |
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