ASN Wikibase Occurrence # 223890
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 11 April 2019 |
Time: | 13:30 LT |
Type: | Cessna 150G |
Owner/operator: | Private |
Registration: | N3795J |
MSN: | 15065095 |
Year of manufacture: | 1966 |
Total airframe hrs: | 3583 hours |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Oswego County, Fulton, NY -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Malone-Dufort Airport, NY (KMAL) |
Destination airport: | Fulton-Oswego County Airport, NY (KFZY) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After descending with the engine power above 2,000 rpm, the pilot entered the traffic pattern for the destination airport. Just after turning onto the base leg of the pattern, the pilot applied the carburetor heat and the engine 'faltered' and lost partial power. The pilot then deactivated the carburetor heat, and the engine regained some power. He reapplied the carburetor heat, and the engine stopped. He attempted to restart the engine but was unsuccessful. While performing a forced landing to a road, the right wing impacted a utility pole and the airplane rolled over and sustained substantial damage to both wings and the fuselage.
The weather conditions at the time of the accident were favorable for carburetor icing at altitude and at the surface. It is likely that carburetor ice developed during the descent; when the pilot applied the carburetor heat while in the traffic pattern, the ice began to melt, which introduced water into the engine intake and resulted in the engine losing partial power. The pilot's subsequent cycling of the carburetor heat at a relatively low power setting likely resulted in the total loss of engine power.
Probable Cause: A total loss of engine power due to carburetor icing. Contributing was the pilot's failure to leave the carburetor heat on fully after his initial application of carburetor heat.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA19LA151 |
Status: | Investigation completed |
Duration: | 2 years and 9 months |
Download report: | Final report |
|
Sources:
NTSB ERA19LA151
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=3795J Location
Revision history:
Date/time | Contributor | Updates |
11-Apr-2019 22:54 |
Geno |
Added |
02-Jul-2022 09:20 |
ASN Update Bot |
Updated [Time, Other fatalities, Nature, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation