ASN Wikibase Occurrence # 224770
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Date: | Sunday 5 May 2019 |
Time: | 08:30 LT |
Type: | Piper PA-34-220T Seneca V |
Owner/operator: | SPC Leasing LLC |
Registration: | N999CR |
MSN: | 3449143 |
Total airframe hrs: | 1819 hours |
Engine model: | Continental TSIO-360 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Anderson Municipal Airport-Darlington Field (KAID), Anderson, IN -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Anderson Municipal Airport, IN (AID/KAID) |
Destination airport: | Huntington Municipal Airport, IN (KHHG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot planned to ferry the twin-engine airplane to another airport for the annual maintenance inspection. Several witnesses saw the airplane's departure. Two of the witness reported that the airplane engines didn't sound "normal". Several witnesses reported that the airplane appeared to pitch up, before stalling.
A video from the airport's security camera revealed that the airplane appeared to climb steeply; the airplane's wings rocked back-and-forth, and the airplane disappeared out of view. When the airplane reappeared in the camera's view, the airplane was in a descent with the left wing low. The airplane collided with terrain and the airplane cabin area was largely destroyed by the impact.
Examination of the airplane found the stabilator trim actuator screw was near its maximum nose up setting. The left engine was removed from the airframe and tested in the engine manufacturers test cell. The engine test run reveled the engine did not produce full rated horsepower and on occasions produced black exhaust which was indicative of a rich fuel air mixture. The fuel servo was replaced with a new unit and the engine was able to produce rated horsepower. Further examination of the original fuel servo showed that the control linkage (rod and link assembly), was installed incorrectly.
The accident is consistent with loss of power on the left engine due to an incorrectly installed fuel servo and an excessive nose up trim setting, which resulted in steep climb angle, a loss of airspeed, and an aerodynamic stall.
Probable Cause: The loss of left engine power due to an incorrectly adjusted fuel servo and the airplane's nose up trim which resulted in the airplane steep climb, loss of airspeed, and aerodynamic stall and subsequent impact with terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19FA135 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=999CR NTSB CEN19FA135
History of this aircraft
Other occurrences involving this aircraft
17 February 2010 |
N999CR |
NuPrairie Packaging Co. |
0 |
St. Paul Downtown Airport / Holman Field, St. Paul, MN |
|
min |
Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
05-May-2019 14:53 |
Geno |
Added |
05-May-2019 16:40 |
RobertMB |
Updated [Aircraft type, Total occupants, Nature, Departure airport, Source, Narrative] |
05-May-2019 16:40 |
RobertMB |
Updated [Phase] |
05-May-2019 18:03 |
Geno |
Updated [Registration, Cn, Operator, Source] |
28-Mar-2021 07:31 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report] |
28-Mar-2021 07:50 |
harro |
Updated [Destination airport, Source, Narrative, Photo] |
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