ASN Wikibase Occurrence # 225996
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Date: | Monday 9 July 2018 |
Time: | 20:20 |
Type: | Robinson R44 |
Owner/operator: | Cedar Ridge Aviation |
Registration: | N144DJ |
MSN: | 2467 |
Year of manufacture: | 2017 |
Total airframe hrs: | 767 hours |
Engine model: | Lycoming O-540-F1B5 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Rulo, NE -
United States of America
|
Phase: | Unknown |
Nature: | Agricultural |
Departure airport: | Rulo, NE |
Destination airport: | Rulo, NE |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the helicopter pilot, he was performing a night agricultural flight. During takeoff from a platform located on top of the tender, his collective application was too aggressive, and during the ascent, the engine sputtered. The engine rpm and main rotor rpm decreased, and he tried to regain the rpm by lowering the collective. The helicopter was moving forward and descending, so he applied aft cyclic to arrest the forward movement, and he attempted to land. The left skid touched down in the soft dirt, and the pilot applied aft cyclic to prevent a nose-over, but the main rotor blades struck the tailboom. The helicopter rolled forward, and its nose spun left before the helicopter came to rest on its left side.
The helicopter sustained substantial damage the fuselage, tail rotor drive system, and skid tubes.
The pilot reported that the accident could have been prevented if he had not been in a hurry to complete the operation and that there were no mechanical malfunctions or failures with the helicopter that would have precluded normal operation.
Probable Cause: The pilot's improper collective application, which resulted in low rotor rpm during the takeoff climb and a subsequent ground collision. Contributing to the accident was the pilot’s self-induced pressure to complete the operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA18CA408 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
10-Jun-2019 06:46 |
ASN Update Bot |
Added |
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