Runway excursion Accident Beechcraft 77 Skipper N1802Y,
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ASN Wikibase Occurrence # 226654
 
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Date:Friday 28 June 2019
Time:10:30 LT
Type:Silhouette image of generic BE77 model; specific model in this crash may look slightly different    
Beechcraft 77 Skipper
Owner/operator:The Villages Flight Club
Registration: N1802Y
MSN: WA-268
Year of manufacture:1983
Total airframe hrs:2090 hours
Engine model:Lycoming O-235-L2C
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Leesburg International Airport (KLEE/LEE), Leesburg, FL -   United States of America
Phase: Landing
Nature:Training
Departure airport:Leesburg International Airport, FL (LEE/KLEE)
Destination airport:Leesburg International Airport, FL (LEE/KLEE)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight instructor was performing a checkout flight with the commercial pilot. They completed about 30 minutes of air work before returning to the airport to practice takeoffs and landings. The first landing was normal, and the commercial pilot added power to take off. When the airplane reached an altitude of 400 ft above the ground, the engine lost partial power and the airplane began to descend. The flight instructor took control of the airplane and landed in trees and a swamp adjacent to the airport. Examination of the engine revealed that it was full of water and debris from immersion in the swamp; however, no mechanical discrepancies were identified that would have precluded normal operation at the time of the accident.
A carburetor icing probability chart indicated that the airplane was operating in an environment associated with a serious risk of carburetor ice accumulation at glide power settings. The flight instructor stated that they did not use carburetor heat before landing because the carburetor heat caused the engine to run very rough when applied. Given that a postaccident examination of the engine revealed no mechanical issues with the engine, and the flight instructor stated that the carburetor heat was not being used during the flight while operating in an environment that was conducive to carburetor icing, the loss of engine power was most likely due to carburetor ice that accumulated during the approach. 
 

Probable Cause: A partial loss of engine power due to carburetor icing, which resulted from the flight instructor's decision not to use carburetor heat.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA19LA217
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB ERA19LA217

Location

Images:


Photo: FAA

Revision history:

Date/timeContributorUpdates
28-Jun-2019 20:30 Captain Adam Added
17-Sep-2019 07:53 harro Updated [Time, Registration, Cn, Source, Narrative]
27-Mar-2021 12:46 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Damage, Narrative, Accident report]
27-Mar-2021 14:48 ASN Update Bot Updated [Departure airport, Destination airport, Damage, Category, Accident report]
27-Mar-2021 15:27 harro Updated [Source, Narrative, Photo]

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