ASN Wikibase Occurrence # 226853
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Date: | Thursday 26 November 2015 |
Time: | 11:45 |
Type: | Robinson R44 II |
Owner/operator: | Timberview Helicopters |
Registration: | N7512N |
MSN: | 10131 |
Year of manufacture: | 2003 |
Total airframe hrs: | 1758 hours |
Engine model: | Lycoming IO-540-AE1A5 |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Destin, FL -
United States of America
|
Phase: | |
Nature: | Unknown |
Departure airport: | Destin, FL (DTS) |
Destination airport: | Destin, FL (DTS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot was performing a power check before an air tour flight with three passengers onboard. While raising the collective, he heard a loud “pop.” He then immediately lowered the collective and secured the helicopter.
Postaccident examination of the helicopter revealed that an overstress fracture existed between the tail rotor driveshaft and intermediate flex plate. Examination revealed that all the hardware was in place except for a washer, which is required at each connection between the clutch shaft yoke and flex plate per a caution in the helicopter’s maintenance manual. The maintenance manual also contained measurements to determine proper shimming required at the intermediate flex plate. A review of maintenance records revealed that, about 11 flight hours before the accident, the sprag clutch had been removed and replaced. The mechanic who performed the clutch removal and installation stated that the measurements he took at the intermediate flex plate during and after his repairs were the same. He also indicated that, when they installed new hardware, he obtained the same dimensions. Although a misalignment of the intermediate flex coupling would place significant tension along the entire length of the driveshaft between the main rotor gearbox and tail rotor gearbox and a missing washer both could have caused a fatigue-type failure of the tail rotor drive line, the parts fractured due to overstress, not fatigue; therefore, it is unlikely that the missing hardware contributed to the failure. The reason for the overstress fracture between the tail rotor driveshaft and intermediate flex plate could not be determined based on the available evidence.
Probable Cause: The overstress fracture between the tail rotor driveshaft and intermediate flex plate for reasons that could not be determined based on the available evidence.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | ERA16LA054 |
Status: | Investigation completed |
Duration: | 3 years and 7 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
06-Jul-2019 19:35 |
ASN Update Bot |
Added |
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