ASN Wikibase Occurrence # 226947
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Date: | Monday 8 July 2019 |
Time: | 16:00 LT |
Type: | Rutan VariEze |
Owner/operator: | Private |
Registration: | N112EZ |
MSN: | 43 |
Year of manufacture: | 1982 |
Total airframe hrs: | 141 hours |
Engine model: | Continental C85-12 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Kane County, NW of Kaneville, IL -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Chicago/Waukegan, IL |
Destination airport: | Alto Rio Senguerr Airport, CB (ARR/SAVR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot of the experimental airplane reported that he was unable to enter the destination airport airspace, so he remained outside of the airspace at a reduced power setting. After adjusting the mixture control, the engine experienced a complete loss of power and the propeller stopped rotating. About 1,600 ft above ground level (agl), the pilot initiated a steep dive to increase airspeed and attempt to get the propeller to windmill and the engine to restart; however, the propeller would not rotate, so he pulled out of the dive about 300 ft agl and aligned with traffic on an interstate for a forced landing. During the landing, the right wing contacted a truck and the airplane sustained substantial damage to the wings and fuselage.
A postaccident engine test run revealed no anomalies, and the test was unable to determine why the propeller would not windmill above the published speed. The atmospheric conditions at the time of the accident were conducive to the accumulation of carburetor icing at glide and cruise power settings. The pilot did not use the carburetor heat during the reduced engine power operation; therefore, it is likely that the carburetor accumulated ice, which resulted in the total loss of engine power.
Probable Cause: The pilot's failure to use carburetor heat while operating at low power settings in conditions conducive to the development of carburetor ice, and the subsequent total loss of engine power due to carburetor icing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19LA216 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
https://flightaware.com/resources/registration/N112EZ NTSB CEN19LA216
Location
Revision history:
Date/time | Contributor | Updates |
08-Jul-2019 23:12 |
Geno |
Added |
08-Jul-2019 23:19 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Location, Source, Narrative] |
09-Jul-2019 00:08 |
Captain Adam |
Updated [Departure airport, Source, Narrative] |
27-Mar-2021 11:04 |
ASN Update Bot |
Updated [Time, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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