Accident Cessna 206 N5152U,
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ASN Wikibase Occurrence # 228105
 
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Date:Friday 9 August 2019
Time:17:20 LT
Type:Silhouette image of generic C206 model; specific model in this crash may look slightly different    
Cessna 206
Owner/operator:Skinner Leasing LLC
Registration: N5152U
MSN: 206-0152
Year of manufacture:1964
Total airframe hrs:15563 hours
Engine model:Continental IO-520-A5B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:E of Rustler Peak, 2 miles SE of Prospect, OR -   United States of America
Phase: Landing
Nature:Fire fighting
Departure airport:Medford-Rogue Valley International, OR (MFR/KMFR)
Destination airport:Medford-Rogue Valley International, OR (MFR/KMFR)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
About 2.8 hours into the fire reconnaissance mission flight, the pilot heard a loud bang followed by violent shaking of the airplane. The pilot believed the airplane was at an altitude of about 1,500-2,000 ft. above the ground. The pilot retarded the propeller control to extend his glide distance while he looked for a place to land. The airplane touched down in a swamp and during the landing, the left wing and fuselage were substantially damaged.
A postaccident examination of the engine revealed extensive damage to the no. 1 cylinder, piston, and connecting rod. The no. 1 cylinder valve guide rods broke through the crankcase, and the rear counterweight and counterweight lobe were broken free from the crankshaft. Numerous metal pieces and shavings were noted in the oil pan including: a broken counterweight, crankshaft counterweight attachment, counterweight retainer pin, damaged retainer pin plates, damaged retainer plate spring clips, and engine casing pieces. One of the damaged retainer pin plates displayed a deep groove, the approximate diameter of a counterweight pin.
It is likely that the counterweight retaining pin rotated over time on the counterweight retainer pin plate, causing it to wear down and eventually fail. When the plate failed, the counterweight retainer pin moved from its position and impacted the no. 1 piston rod, causing the counterweight lobe to fracture and the engine to lose power.

Probable Cause: The failure of the counterweight retainer pin plate which resulted in a total loss of engine power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR19LA217
Status: Investigation completed
Duration: 2 years and 9 months
Download report: Final report

Sources:

NTSB WPR19LA217

https://flightaware.com/live/flight/N5152U

FAA register: https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N5152U

Location

Revision history:

Date/timeContributorUpdates
11-Aug-2019 14:29 Aerossurance Added
11-Aug-2019 15:06 RobertMB Updated [Operator, Nature]
11-Aug-2019 19:36 Geno Updated [Operator, Phase, Departure airport, Destination airport, Source]
01-Jul-2022 19:23 ASN Update Bot Updated [Time, Operator, Other fatalities, Source, Damage, Narrative, Category, Accident report]

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