ASN Wikibase Occurrence # 228562
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Date: | Tuesday 27 August 2019 |
Time: | 11:06 LT |
Type: | Beechcraft 35 Bonanza |
Owner/operator: | Private |
Registration: | N6245V |
MSN: | D-8581 |
Year of manufacture: | 1967 |
Total airframe hrs: | 4873 hours |
Engine model: | Continental IO-520-BA |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Monroe Municipal Airport (EFT/KEFT), Green County, WI -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Rochester International Airport, MN (RST/KRST) |
Destination airport: | Chicago-Midway Airport, IL (MDW/KMDW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot and passenger were en route on an instrument flight rules flight when the engine lost oil pressure, followed by a total loss of engine power. The pilot declared an emergency with air traffic control and stated that he 'had an oil pressure event there but it's building back up so standby.' The controller cleared him direct to the nearest airport and asked the pilot if he need any assistance at the airport, which the pilot declined. Flight track data showed that the airplane began a shallow descent toward the diversion airport before the data ended about 2 minutes later. The pilot stated that he flew directly over the airport and was unable to see it due to oil on the windshield and smoke in the cabin; he eventually performed a forced landing in a field about 4 nautical miles from the diversion airport.
A postaccident disassembly examination revealed a large hole in the top of the engine crankcase above the No. 6 cylinder. The inside of the engine contained a significant amount of metallic debris. The Nos. 1 through 4 connecting rods remained attached to the crankshaft, but all exhibited significant heat distress from a lack of oil lubrication. The Nos. 5 and 6 connecting rods fractured at the bearing and sustained damage from impacting the crankshaft, cylinder walls, and the inside of the case. The ends of the Nos. 5 and 6 connecting rods and their bearings were not found or identified within the available metallic debris. It is likely that the Nos. 5 and 6 connecting rods failed due to a lack of oil lubrication; however, the reason for the oil loss could not be determined. The continued operation of the engine after the loss of oil pressure likely contributed to and aggravated the amount of damage to the engine.
Probable Cause: A total loss of engine power due to the failure of the Nos. 5 and 6 connecting rods from a lack of oil lubrication for reasons that could not be determined.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19LA290 |
Status: | Investigation completed |
Duration: | 2 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB CEN19LA290
https://flightaware.com/live/flight/N6245V/history/20190827/1550Z/KRST/KMDW https://flightaware.com/photos/view/499447-facd84bd5bd5afd8a1faac6acd3a4220c7541342 (photo)
Location
Revision history:
Date/time | Contributor | Updates |
27-Aug-2019 21:03 |
Captain Adam |
Added |
27-Aug-2019 23:45 |
RobertMB |
Updated [Time, Aircraft type, Registration, Cn, Operator, Location, Departure airport, Destination airport, Source, Damage, Narrative] |
01-Jul-2022 18:44 |
ASN Update Bot |
Updated [Time, Other fatalities, Source, Damage, Narrative, Category, Accident report] |
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