ASN Wikibase Occurrence # 228774
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Date: | Friday 6 September 2019 |
Time: | 10:09 LT |
Type: | Piper PA-18-150 Super Cub |
Owner/operator: | Pa-18 LLC |
Registration: | N14365 |
MSN: | 18-7409092 |
Year of manufacture: | 1974 |
Total airframe hrs: | 6142 hours |
Engine model: | Lycoming O-360-A4A |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ken Jernstedt Airfield (4S2), Hood River, OR -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Hood River, OR |
Destination airport: | Hood River, OR |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Witnesses observed the airplane takeoff, and one witness noted its nose-high attitude during takeoff. They then heard the engine lose power. The airplane subsequently pitched down and began a rotation to the right before impacting the ground just north of the runway.
First responders reported that the fuel selector valve was found in the OFF position when they arrived at the accident site, and they also noted fuel leaking from the airplane. Further examination of the airplane revealed the fuel selector indicator plate displayed a red witness mark adjacent to the fuel selector pointer under one of the OFF-indicator marks, which is an indication the selector was in the OFF position at the time of impact. No evidence of mechanical malfunctions or failures were identified that would have precluded normal operation. Because the engine lost power during takeoff, it is possible that there was enough residual fuel in the fuel lines to start the engine and taxi to the runway, even with the selector in the OFF position.
The private pilot was seated in the front seat and the certified flight instructor was seated in the rear seat. The fuel selector was located on the left cabin wall closest to the private pilot; it is likely the private pilot failed to check the position before takeoff.
When the airplane departed, it was about 21 pounds over the maximum takeoff weight. An increase in the airplane's weight would have an adverse effect on stability and controllability. Because the airplane was already in a nose-high attitude when the engine lost power, the airplane likely stalled. The increased weight and low altitude when the power loss occurred prevented the pilots from recovering.
Postmortem toxicology testing detected quinine in the certified flight instructor's blood and urine at a level that was not quantified; therefore, the amount detected was likely from a tonic drink containing quinine rather than ingestion of the drug and would not have been impairing.
Probable Cause: The total loss of engine power shortly after takeoff as a result of the private pilot's failure to ensure the fuel selector was in the appropriate position and the certified flight instructor's exceedance of the airplane's critical angle of attack at the time of the engine power loss, which resulted in an aerodynamic stall and loss of airplane control.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR19FA251 |
Status: | Investigation completed |
Duration: | 3 years |
Download report: | Final report |
|
Sources:
NTSB WPR19FA251
Location
Revision history:
Date/time | Contributor | Updates |
06-Sep-2019 21:07 |
Geno |
Added |
06-Sep-2019 21:23 |
RobertMB |
Updated [Aircraft type, Registration, Cn, Operator, Nature, Source, Damage, Narrative] |
09-Sep-2022 13:57 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report] |
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