Fuel exhaustion Accident Taylorcraft BC-12-D N95131,
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ASN Wikibase Occurrence # 229569
 
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Date:Tuesday 1 October 2019
Time:10:55 LT
Type:Silhouette image of generic TAYB model; specific model in this crash may look slightly different    
Taylorcraft BC-12-D
Owner/operator:N95131 Aviation LLC
Registration: N95131
MSN: 9531
Year of manufacture:1959
Total airframe hrs:4791 hours
Engine model:Continental A65-8
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Longs, north of Grand Strand Airport (KCRE), North Myrtle Beach, SC -   United States of America
Phase: Landing
Nature:Private
Departure airport:Forest, VA (W90)
Destination airport:North Myrtle Beach, SC
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that, during preflight preparations, he estimated that the flight time would be about 2 hours 29 minutes with a total fuel burn of 10.1 gallons. The airplane departed with 12 gallons of fuel. About 2 hours 25 minutes into the flight, the engine quit. The pilot navigated toward a nearby field to make an off-airport landing. During the landing, he saw a deep ditch and a house, so he attempted to ground loop the airplane to the left. Both wings impacted trees. The airplane sustained substantial damage to both wings. The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation. The pilot reported as a safety recommendation that adding a fuel stop would have prevented the accident.

The Federal Aviation Administrator inspector who examined the airplane reported that the nose tank had evidence of fuel being in it recently (the indicator cork was still wet with fuel), but no fuel remained in the tank. Both the right and left wing tanks were examined, and no fuel remained in either tank. No evidence of a fuel spill was found on the airplane or the ground.

Probable Cause: The pilot's improper fuel planning, which resulted in fuel exhaustion, a total loss of engine power, an off-airport landing, and impact with trees.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: GAA20CA001
Status: Investigation completed
Duration:
Download report: Final report

Sources:


FAA register: https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N95131

NTSB GAA20CA001

Location

Images:


Photo: FAA

Revision history:

Date/timeContributorUpdates
01-Oct-2019 18:22 Captain Adam Added
01-Oct-2019 19:35 harro Updated [Aircraft type]
02-Oct-2019 00:14 Geno Updated [Time, Location, Phase, Source, Narrative]
02-Oct-2019 09:06 A.J.Scholten Updated [Source]
26-Mar-2021 20:45 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report]
26-Mar-2021 21:04 harro Updated [Source, Narrative, Photo]

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