ASN Wikibase Occurrence # 230365
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Date: | Thursday 15 November 2018 |
Time: | |
Type: | de Havilland Canada DHC-8-402Q Dash 8 |
Owner/operator: | Flybe |
Registration: | G-JECR |
MSN: | 4139 |
Year of manufacture: | 2006 |
Engine model: | Pratt & Whitney Canada PW150A |
Fatalities: | Fatalities: 0 / Occupants: 39 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Exeter Airport (EXT/EGTE) -
United Kingdom
|
Phase: | En route |
Nature: | Passenger - Scheduled |
Departure airport: | Exeter Airport (EXT/EGTE) |
Destination airport: | Paris-Charles de Gaulle Airport (CDG/LFPG) |
Investigating agency: | AAIB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Whilst climbing to FL190 en-route to Paris-Charles de Gaulle Airport, the pilots received an alt mismatch message and they elected to return to Exeter Airport. Following an inspection after landing, a small white crystalline deposit was found covering three of the four static pressure holes on the left primary pitot static probe.
It is probable that the use of a non-approved product, to improve the seal between a test adaptor and the pitot static probe during maintenance immediately prior to this flight, may have resulted in the blockage of the static holes and led to the altitude mismatch message.
The investigation found that a non-approved product was probably used to improve the seal between a testing device and the probe during maintenance immediately before the flight, and this may have resulted in the blockage of the static holes, leading to the altitude mismatch message. Two Safety Recommendations have been made to prevent similar incidents. The maintenance organisation has taken safety action to introduce tighter controls on the test kit equipment.
Accident investigation:
|
| |
Investigating agency: | AAIB |
Report number: | EW/C2018/11/01 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
http://aerossurance.com/safety-management/q400-test-kit-wad-wai/ https://www.gov.uk/government/news/aaib-report-dash-8-q400-serious-incident-and-returned-to-exeter
History of this aircraft
Other occurrences involving this aircraft
3 February 2016 |
G-JECR |
Flybe |
0 |
En route, between Birmingham and Aberdeen |
|
min |
Loss of pressurization |
29 August 2016 |
G-JECR |
FlyBe |
0 |
Birmingham International Airport (BHX/EGBB) |
|
min |
Tire failure |
Media:
#OTD 2018 #AAIB safety investigation revealed a difference between 'work as imagined' and 'work as done' in testing the pitot static system.
http://aerossurance.com/safety-management/q400-test-kit-wad-wai/ #aviationmaintenance #humanfactors #aviationsafety #flightsafety
Revision history:
Date/time | Contributor | Updates |
02-Nov-2019 18:54 |
harro |
Added |
09-Nov-2019 21:57 |
Dr. John Smith |
Updated [Location, Source, Embed code, Narrative] |
06-Dec-2019 21:26 |
Aerossurance |
Updated [Location, Source, Embed code] |
13-Dec-2019 20:18 |
harro |
Updated [Source, Accident report, ] |
15-Nov-2020 11:14 |
Aerossurance |
Updated [Embed code, Accident report] |
24-Dec-2021 17:47 |
harro |
Updated [Accident report] |
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