Accident Bellanca 7KCAB Citabria N36339,
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ASN Wikibase Occurrence # 236940
 
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Date:Friday 12 June 2020
Time:09:00 LT
Type:Silhouette image of generic CH7B model; specific model in this crash may look slightly different    
Bellanca 7KCAB Citabria
Owner/operator:Boeing Employees Flying Assoc Inc
Registration: N36339
MSN: 388-73
Year of manufacture:1973
Total airframe hrs:5961 hours
Engine model:Lycoming IO-320-E2A
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Renton, WA -   United States of America
Phase: Initial climb
Nature:Training
Departure airport:Renton Airport, WA (RNT/KRNT)
Destination airport:Renton Airport, WA (RNT/KRNT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane had recently undergone an annual inspection, and the accident flight was the first flight since being out of maintenance. After making a normal departure and touch-and-go landing, the pilot receiving instruction applied full power. As the airplane reached an altitude of about 400 feet above ground level (agl), the engine abruptly stopped producing (total) power. The airplane could not maintain level altitude and during the subsequent off-airport landing, the airplane was substantially damaged when it collided with a tree.

Postaccident examination revealed that the air induction box contained a piece of bunched up paper that likely restricted the inlet cavity. As part of the annual inspection, a repair person completed a small fiberglass patch and painting on the lower cowling. He could not recall the specific repair on the airplane but said he often placed paper in the induction to prevent debris from entering the engine. After the maintenance, the airplane sat for a day with the lower cowling not fastened but maintenance personnel did not recognize the blockage. They also did not find the paper during the post-maintenance inspections and returned the airplane into service with an unsafe condition.

Probable Cause: Maintenance personnel's inadequate post-maintenance inspections that resulted in the total loss of engine power due to a blockage in the air intake.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR20LA180
Status: Investigation completed
Duration: 1 year and 10 months
Download report: Final report

Sources:

NTSB WPR20LA180

History of this aircraft

Other occurrences involving this aircraft
11 January 1987 N36339 James Skinner 0 Bremerton, WA sub

Location

Revision history:

Date/timeContributorUpdates
12-Jun-2020 19:22 Captain Adam Added
12-Jun-2020 21:10 RobertMB Updated [Aircraft type, Registration, Cn, Operator, Nature, Departure airport, Destination airport, Source, Narrative]
14-Jun-2020 06:15 Anon. Updated [Phase, Narrative]
25-Jun-2021 17:23 aaronwk Updated [Time, Phase, Nature, Source, Narrative]
01-Jul-2022 09:09 ASN Update Bot Updated [Time, Operator, Other fatalities, Source, Narrative, Category, Accident report]

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