ASN Wikibase Occurrence # 237608
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Date: | Wednesday 1 July 2020 |
Time: | 18:32 LT |
Type: | Piper PA-28-140 Cherokee |
Owner/operator: | Private |
Registration: | N6530W |
MSN: | 28-20609 |
Year of manufacture: | 1964 |
Total airframe hrs: | 2702 hours |
Engine model: | Lycoming O-320-E2A |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Wise County, Bridgeport, TX -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Bridgeport, TX (XBP) |
Destination airport: | Bridgeport, TX (XBP) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported the engine seemed to lose power shortly after takeoff. His attempts to restore engine power were not successful, and he executed a forced landing. A postaccident engine examination revealed evidence of an insect (mud dauber) nest within the carburetor heat induction system.
The pilot purchased the airplane 2 days before the accident. Airplane maintenance records indicated that an annual inspection was completed on the day the airplane was sold to the accident pilot. The records also indicated the airplane had not been flown between the annual inspection in 2017 and the most recent inspection 2 days before the accident. Furthermore, the markings on the oil filter suggested that the oil was not changed during the most recent annual inspection. The airplane was operated 1.16 hours since that most recent inspection.
The insect nest in the carburetor heat system likely became dislodged during airplane operation and subsequently restricted air flow to the carburetor resulting in a loss of engine power. The location of the insect nest was not in an area visible to the pilot during a preflight inspection. However, the presence of the nest could have been detected during a thorough and complete annual maintenance inspection. In addition, the failure of the mechanic to change the engine oil and filter during the most recent annual inspection suggested that the inspection was less than thorough and complete.
Although there was a slight possibility of carburetor icing at glide and cruise power, it is unlikely to have been the cause of the power loss since the loss of engine power occurred shortly after takeoff.
Probable Cause: Maintenance personnel's inadequate inspection, which resulted in a total loss of engine power due to a restricted air intake-induction system.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN20LA258 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB CEN20LA258
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N6530W
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
03-Jul-2020 05:55 |
Geno |
Added |
01-Jul-2022 09:07 |
ASN Update Bot |
Updated [Time, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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