ASN Wikibase Occurrence # 238485
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 10 August 2019 |
Time: | 10:55 LT |
Type: | Bell 206L-1 LongRanger II |
Owner/operator: | Arctic Air |
Registration: | SE-JOA |
MSN: | 45548 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Minor |
Category: | Accident |
Location: | Vuoggatjålme, Norrbotten County -
Sweden
|
Phase: | Initial climb |
Nature: | Ferry/positioning |
Departure airport: | Vuoggatjålme |
Destination airport: | |
Investigating agency: | SHK |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The purpose of the flight was for the pilot to collect and transport six people who were staying around seven minutes’ flying time from the helicopter base. Prior to take-off, there was around 100 litres of fuel in the tank. After flying a couple hundred metres and at an altitude of around 25 metres, the helicopter started suffering yaw disturbances and a little later lost rotor rpm and lift. Because of the low altitude and speed, the pilot maintained the current collective pitch. Consequently, landing was performed with a little speed in the forward direction, which resulted in the landing gear braking against the soft ground and initially causing the helicopter to tip forward, before it returned to a level position. At the low rotor speed that remained following contact being made with the ground, the cyclic position, combined with the nose-down movement resulted in the downwind rotor blade coming into contact with the tail boom, which was then cut off by the rotor blade. The pilot has stated that he is
uncertain about whether he shut down the engine himself or if it stalled because of the engine problem.
The technical examinations of the helicopter and the engine did not show anything that could have caused the loss of engine power. Nor could the loss of power be recreated during test run.
It can be established from the engine parameters that a problem in the form of fluctuations in the engine’s torque (TRQ) arose during the flight. The major loss of power occurred immediately after these fluctuations.
The turbine outlet temperature (TOT) rose sharply in a later phase, which indicates that, at this stage, the engine was receiving an increased flow of fuel and that it was not completely shut down.
The data that has been analysed does not suggest that the loss of power was caused by the actions of the pilot.
The accident was caused by a major loss of engine power occurring in a flight phase in which the chances of landing safely were restricted by the low speed and altitude.
It has not been possible to establish the cause of the loss of engine power. This was probably a consequence of a temporary partial blockage of the fuel supply to the engine.
Accident investigation:
|
| |
Investigating agency: | SHK |
Report number: | L-110/19 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
SHK
Revision history:
Date/time | Contributor | Updates |
22-Jul-2020 14:53 |
harro |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation