Accident Eurocopter AS 350B2 Ecureuil N160SH,
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ASN Wikibase Occurrence # 240501
 
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Date:Tuesday 25 August 2020
Time:07:09
Type:Silhouette image of generic AS50 model; specific model in this crash may look slightly different    
Eurocopter AS 350B2 Ecureuil
Owner/operator:Soloy Helicopters
Registration: N160SH
MSN: 2739
Year of manufacture:1993
Total airframe hrs:7203 hours
Engine model:Honeywell Aerospace LTS101-700D2
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Tuxedni Bay, AK -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Passenger - Non-Scheduled/charter/Air Taxi
Departure airport:Ninilchik, AK
Destination airport:Ninilchik, AK
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On August 25, 2020, about 0709 Alaska daylight time, a Eurocopter (Airbus) AS350 B2 helicopter, N160SH, was substantially damaged when it was involved in an accident near Ninilchik, Alaska. The commercial pilot sustained minor injuries. The helicopter was operated as a Title 14 Code of Federal Regulations Part 135 air taxi flight.

The pilot reported that he was transporting workers to and from various mining sites about 3 miles from the main camp. The pilot flew to a high mountainside helipad, which was located about 2,750 ft mean-sea-level (msl) cut into a rocky steep slope and disembarked 2 passengers. He flew the helicopter to a nearby site and waited a short time for the off going workers to be ready for pick up. He departed and made another approach to the helipad. The pilot stated that when the helicopter was about 25 ft from the landing site, at very slow forward airspeed, the engine "flamed out" and the helicopter yawed right. The pilot continued the right turn, lowered the collective and attempted to autorotate to a level area about 600 ft below the helipad. When the pilot realized that the helicopter could not make the intended site, he slowed down by applying some aft cyclic and increasing collective to cushion the touchdown. The helicopter landed on the skids facing down the mountain and continued to slide. The left skid impacted a rock and the helicopter rolled over and continued down the mountain, resulting in the tail boom separating. The helicopter came to rest on a drill pad under construction about 200 ft below the helipad. The tail section, fuselage and main rotor blades sustained substantial damage. The examination of the airframe did not reveal any discrepancies. The engine was placed on an engine test cell and two tests were run for a total of 2 hours 23 minutes with 9 starts. The engine demonstrated normal operation during testing. No abnormal engine operation, uncommanded shutdown, or loss of power control was observed.

Probable Cause: A loss of engine power for an undetermined reason.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC20LA083
Status: Investigation completed
Duration: 3 years 1 month
Download report: Final report

Sources:

NTSB ANC20LA083

Location

Images:


Revision history:

Date/timeContributorUpdates
26-Aug-2020 13:12 Captain Adam Added
26-Aug-2020 13:32 RobertMB Updated [Aircraft type]
02-Mar-2021 18:10 rudy Updated [[Aircraft type]]
02-Mar-2021 18:10 rudy Updated [[[Aircraft type]]]
07-May-2021 11:57 harro Updated [[[[Aircraft type]]]]
30-Sep-2023 12:20 ASN Update Bot Updated [[[[[Aircraft type]]]]]
30-Sep-2023 12:24 harro Updated [[[[[[Aircraft type]]]]]]

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