Accident Bellanca 17-30A Viking N28067,
ASN logo
ASN Wikibase Occurrence # 245325
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Wednesday 2 December 2020
Time:22:15 LT
Type:Silhouette image of generic BL17 model; specific model in this crash may look slightly different    
Bellanca 17-30A Viking
Owner/operator:Private
Registration: N28067
MSN: 79-30966
Year of manufacture:1979
Total airframe hrs:3187 hours
Engine model:Continental IO-550F4
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Arden Hills, MN -   United States of America
Phase: Landing
Nature:Private
Departure airport:Minneapolis-Anoka County-Blaine Arpt(Janes Field) Airport, MN (KANE)
Destination airport:Arden Hills, MN
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that he heard a loud 'bang' and the engine began to vibrate and ultimately lost complete power. He executed a forced landing to a highway during which the airplane struck a car and a highway divider which resulted in substantial damage to both wings.
Postaccident engine examination revealed that the Nos. 5 and 6 connecting rods had failed. Further examination revealed two undamaged rod nuts within the oil pan that had no remnant of a rod bolt within the threaded portion of the nut. Additionally, a rod bolt, although damaged, was complete from bolt head to threaded shank and did not have a nut on the threaded portion.
Review of maintenance records revealed that the Nos. 1, 4, and 6 cylinders had been removed and replaced due to low compression about 8 years and 396 hours before the accident, but it is not known if the connecting rods were removed at this same time. The most recent engine overhaul was completed 16 years before the accident, and it had accumulated about 1,296 hours time-in-service since the overhaul.
Based on the available evidence, the loss of engine power was likely due to improper connecting rod installation that resulted in the loss of connecting rod bolt torque, separation of the rod bolt nuts, and subsequent failure of the Nos. 5 and 6 connecting rods.

Probable Cause: Incorrect connecting rod installation, which resulted in the failure of the nos. 5 and 6 connecting rods and subsequent total loss of engine power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN21LA073
Status: Investigation completed
Duration: 1 year and 10 months
Download report: Final report

Sources:

NTSB CEN21LA073
https://flightaware.com/resources/registration/N28067


Location

Revision history:

Date/timeContributorUpdates
03-Dec-2020 03:44 Captain Adam Added
03-Dec-2020 04:52 Geno Updated [Time, Aircraft type, Registration, Cn, Operator, Total occupants, Source]
03-Dec-2020 06:40 RobertMB Updated [Time, Total occupants, Location, Nature, Source, Narrative]
03-Dec-2020 06:58 Anon. Updated [Total occupants, Source]
03-Dec-2020 10:00 RobertMB Updated [Location, Nature, Source, Damage, Narrative]
03-Dec-2020 16:38 Captain Adam Updated [Location, Damage, Narrative]
03-Dec-2020 17:05 RobertMB Updated [Location, Damage, Narrative]
03-Dec-2020 18:54 Captain Adam Updated [Damage, Narrative]
14-Oct-2022 12:30 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org