Accident Cessna T182T Turbo Skylane N291FR,
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ASN Wikibase Occurrence # 247329
 
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Date:Sunday 31 January 2021
Time:11:44 LT
Type:Silhouette image of generic C182 model; specific model in this crash may look slightly different    
Cessna T182T Turbo Skylane
Owner/operator:Morey's West Coast Adventures, Inc
Registration: N291FR
MSN: T18209082
Year of manufacture:2012
Total airframe hrs:1787 hours
Engine model:Lycoming TIO-540-AK1A
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:near Lake Earl, NE of Crescent City, CA -   United States of America
Phase: En route
Nature:Training
Departure airport:Medford-Rogue Valley International, OR (MFR/KMFR)
Destination airport:Crescent City-McNamara Field, CA (CEC/KCEC)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight instructor noticed a flashing red turbine inlet temperature (TIT) warning light during the flight. He enrichened the fuel mixture, which returned the TIT to normal. Shortly after, the engine began to run rough. The flight instructor switched to the left magneto and the engine lost power. He then switched to the right magneto and the engine continued to run rough. He switched back to both magnetos and the engine continued to run rough. The flight instructor then adjusted the mixture and turned on the auxiliary fuel pump. Despite his actions, he was unable to get the engine to operate at a power setting sufficient to maintain altitude. The flight instructor located an open field and initiated a forced landing. The airplane landed in marshland and nosed over during the landing.
The postaccident examination of the engine revealed excessive gap on all sparkplugs and two of the sparkplug electrodes were fouled. The magnetos would not produce spark and had corrosion on their internal components. It was also noted that the pressurized magnetos did not have a moisture trap or filter installed.
The magnetos were sent to a facility for further examination, which revealed deformities on both magneto point assembly contact areas and the failure of both magneto capacitors during testing. The failure of the capacitors likely resulted in the deformities on the points surface contact areas resulting in the magnetos not producing sufficient spark for normal operation.

Probable Cause: The partial loss of engine power due to the failure of both magneto capacitors.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR21LA098
Status: Investigation completed
Duration: 2 years and 2 months
Download report: Final report

Sources:

NTSB WPR21LA098
FAA register: https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=N291FR

https://flightaware.com/live/flight/N291FR/history/20210131/1830Z/KMFR/KCEC


Location

Revision history:

Date/timeContributorUpdates
01-Feb-2021 06:44 Geno Added
03-Feb-2021 19:52 RobertMB Updated [Location, Phase, Source]
09-Jul-2021 19:24 aaronwk Updated [Time, Nature, Source, Narrative, Category]

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