Accident Aero Commander 500S Shrike Commander N19WL,
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ASN Wikibase Occurrence # 24920
 
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Date:Monday 14 April 2003
Time:11:40
Type:Silhouette image of generic AC50 model; specific model in this crash may look slightly different    
Aero Commander 500S Shrike Commander
Owner/operator:Private
Registration: N19WL
MSN: 3160
Year of manufacture:1973
Total airframe hrs:11617 hours
Engine model:Lycoming IO-540-E1B5
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Mount Pleasant -   United States of America
Phase: Unknown
Nature:Unknown
Departure airport:Mount Pleasant, SC (8S5)
Destination airport:Mount Pleasant, SC (8S5)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the pilot, he requested the refueler to top off his fuel tanks with "100 low lead fuel". After refueling, the pilot performed a preflight including taking fuel samples from under the wings, draining the rear fuel drain, and checking the fuel cap for security. The engine start, run-up, and taxi were uneventful. The airplane departed runway 17 and was in a positive rate of climb. At approximately 200 feet AGL the airplane began to lose power. Shortly after the pilot ensured that the throttle, propeller, and mixture controls were in the full forward position, the airplane lost power in both engines. The pilot executed an emergency off field landing. Examination of the wreckage revealed that the left wing had broken off and the aft cabin area was crushed. According to the refueler, he stated that he mistakenly used the Jet-A fuel truck instead of the AVGAS 100 low lead truck, and pumped 58 gallons of Jet-A into the airplane. Examination of the fuel samples taken from both engines revealed the left and right engine contained 70 percent of jet A fuel.

Probable Cause: The improper refueling of the airplane by airport personnel with the incorrect fuel grade that resulted in a total loss in engine power on both engines during initial climb. A factor was the inadequate preflight inspection by the pilot in command.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL03TA078
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20030416X00520&key=1

Location

Revision history:

Date/timeContributorUpdates
27-Sep-2008 01:00 ASN archive Added
21-Dec-2016 19:14 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:16 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:20 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
08-Dec-2017 18:32 ASN Update Bot Updated [Cn, Operator, Nature, Departure airport, Destination airport, Source, Narrative]

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