ASN Wikibase Occurrence # 264942
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Date: | Wednesday 30 June 2021 |
Time: | 18:00 LT |
Type: | Aeronca 15AC Sedan |
Owner/operator: | Private |
Registration: | N1175H |
MSN: | 15AC-188 |
Year of manufacture: | 1948 |
Total airframe hrs: | 2875 hours |
Engine model: | Continental O-300 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hastings Airport, MI (9D9) -
United States of America
|
Phase: | Approach |
Nature: | Training |
Departure airport: | Hastings Airport, MI (9D9) |
Destination airport: | Hastings Airport, MI (9D9) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot receiving instruction and flight instructor were conducting a flight review. About 45 minutes into the flight, the engine “sputtered' and lost power following a practice go-around. The flight instructor took control of the airplane and performed a forced landing, during which the airplane sustained substantial damage. The pilot reported that they departed on the flight with 8 gallons of fuel in the left-wing tank and 7 gallons of fuel in the right-wing tank. The flight instructor recalled that, shortly before the loss of engine power, the left and right tanks contained about 8 gallons and 2 gallons, respectively. The mechanic who recovered the airplane reported that about 6 gallons remained in the left fuel tank and 2 gallons in the right fuel tank. The fuel caps were secure, and the accident site did not exhibit any evidence of a fuel spill.
A postaccident examination and engine test run did not reveal any anomalies consistent with a preimpact failure or malfunction. Continuity of the airframe fuel system was confirmed. The reason that fuel was being drawn predominantly from the right fuel tank could not be determined. The reason for the loss of engine power could not be determined based on the available information.
Probable Cause: A total loss of engine power for reasons that could not be determined based on the available information.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN21LA303 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB CEN21LA303
FAA register:
https://registry.faa.gov/aircraftinquiry/Search/NNumberResult?nNumberTxt=1175H https://flightaware.com/live/flight/N1175H/history/20210630/2116Z/9D9/9D9 Location
Revision history:
Date/time | Contributor | Updates |
01-Jul-2021 03:23 |
Geno |
Added |
01-Jul-2021 07:35 |
RobertMB |
Updated [Aircraft type, Registration, Cn, Operator, Departure airport, Destination airport, Source, Damage, Narrative] |
01-Jul-2021 16:33 |
Captain Adam |
Updated [Damage, Narrative] |
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