ASN Wikibase Occurrence # 26716
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Date: | Monday 26 March 2001 |
Time: | 07:19 |
Type: | Socata TBM700 |
Owner/operator: | Technical Leasing, Inc. |
Registration: | N300WC |
MSN: | 82 |
Year of manufacture: | 1993 |
Total airframe hrs: | 5139 hours |
Engine model: | P&W Canada PT6A-64 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | 1/4 mile S of Centennial Airport, Englewood, Colorado -
United States of America
|
Phase: | Take off |
Nature: | Executive |
Departure airport: | Englewood, CO (APA) |
Destination airport: | Santa Monica, CA (SMO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was fueled to capacity and placed in a heated hangar about one hour before departure. The instrument rated pilot obtained a weather briefing, filed an IFR flight plan, and obtained an IFR clearance. Low ceiling, reduced visibility, and ice fog prevented control tower personnel from observing the takeoff. Radar (NTAP) and on-board GPS data indicated the airplane began drifting to the left of runway centerline almost immediately after takeoff. The airplane made a climbing left turn, achieving a maximum altitude of 7,072 feet and completing 217 degrees of turn, before beginning a descending left turn. The airplane impacted terrain on airport property. Autopsy/toxicology protocols were unremarkable. There was no evidence of preimpact failure/malfunction of the airframe, powerplant, propeller, or flight controls. The autopilot and servos, pitot-static system, and flight instruments were tested and all functioned satisfactorily. The pilot's shoulder harness was found attached to the seatbelt, but the male end of the seatbelt buckle was broken.
Probable Cause: the pilot's spatial disorientation, which led to his failure to maintain aircraft control. A contributing factor was the pilot's decision to intentionally fly into known adverse weather that consisted of low ceilings, obscuration, and ice fog.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN01FA075 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20010328X00660&key=1 FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?omni=Home-N-Number&nNumberTxt=300WC Location
Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
11-Mar-2014 15:04 |
wf |
Updated [Cn, Location, Phase, Departure airport, Destination airport, Source, Damage, Narrative] |
30-Jul-2016 22:46 |
Dr.John Smith |
Updated [Time, Location, Nature, Departure airport, Destination airport, Source, Narrative] |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Dec-2017 10:48 |
ASN Update Bot |
Updated [Operator, Nature, Departure airport, Destination airport, Source, Narrative] |
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