Accident Piper PA-28R-201 N9185P,
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ASN Wikibase Occurrence # 268843
 
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Date:Wednesday 20 December 2000
Time:10:25 LT
Type:Silhouette image of generic P28R model; specific model in this crash may look slightly different    
Piper PA-28R-201
Owner/operator:
Registration: N9185P
MSN: 28R-7837032
Total airframe hrs:5342 hours
Engine model:Lycoming IO-360-C1C6
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Minor
Category:Accident
Location:FORT PIERCE, Florida -   United States of America
Phase: Unknown
Nature:Private
Departure airport:(FPR)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that when he turned off the electric fuel boost pump after takeoff, the engine lost about 300 rpm. He turned the electric pump back on and the engine regained power. While turning on final approach for landing he lined up with the wrong runway and made a go-around. During the go-around, the engine popped and went to idle power. He was unable to return to the airport and landed in a field. During landing rollout, the nose landing gear collapsed and he hit his head when the shoulder harness did not lock. The airplane received minor damage in the accident and the pilot was hospitalized for a head injury. Postcrash running of the engine showed no evidence of failure or malfunction with the electric boost pump on or off. The pilot's shoulder harness was found stowed after the accident and it locked normally during pull tests. The pilot was under a court order dated June 4, 1998, to not operate aircraft, and was scheduled to surrender to authorities in the State of Connecticut to begin serving a prison sentence on the day of the accident.

Probable Cause: The pilot's improper approach for landing while making a landing following a reported momentary partial loss of engine power for undetermined reasons and his decision to make a go-around from the approach resulting in a landing in a field and collapse of the nose landing gear following a reported total loss of engine power for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA01LA048
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB MIA01LA048

Revision history:

Date/timeContributorUpdates
15-Oct-2021 12:34 ASN Update Bot Added

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