Accident Robinson R22 N7187W,
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ASN Wikibase Occurrence # 268850
 
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Date:Sunday 17 December 2000
Time:11:40 LT
Type:Silhouette image of generic R22 model; specific model in this crash may look slightly different    
Robinson R22
Owner/operator:
Registration: N7187W
MSN: 0955M
Year of manufacture:1989
Engine model:Lycoming O-320-B2C
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Sunnyvale, TX -   United States of America
Phase: Unknown
Nature:Training
Departure airport:MESQUITE , TX (HQZ)
Destination airport:GARLAND , TX (T57)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While en route at 1,000 feet agl, the instructor pilot gave the student a simulated engine failure over a field and instructed the student to make an autorotation with a power recovery. The student pilot made a gradual 360-degree turn while descending to the field. The instructor stated that the student leveled the helicopter on final approach. The instructor made one last search for obstacles, and looked back into the cockpit to find the airspeed was at 45 knots and the main rotor RPM was at the bottom of the green arc (approximately 97%). The helicopter was approximately 100 feet agl when the instructor pilot took over control of the helicopter and attempted a 'high power recovery.' He rolled on the throttle, pulled up on the collective, felt a 'slight hesitation,' and the helicopter then 'snapped to the right.' At that time, the instructor applied left pedal and heard the low rotor RPM warning horn. The instructor stated that he thought that the helicopter did not touch down level due to the rotation to the right. The helicopter touched down in the field, 'hopped to the right approximately 40 degrees' and then became airborne again. The instructor stated that he thought that he still had either full throttle applied to the engine and/or the collective raised. As the helicopter became airborne, it rotated 360 degrees to the right, contacted the ground with the tail rotor, then the right skid. Subsequently, the helicopter rolled over onto its right side.

Probable Cause: The flight instructor's inadequate supervision of his student and his failure to maintain control of the helicopter. Factors were the student pilot allowing the airspeed and main rotor RPM to get too low during the simulated emergency.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW01LA039
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB FTW01LA039

Revision history:

Date/timeContributorUpdates
15-Oct-2021 12:36 ASN Update Bot Added
05-Jul-2022 12:51 Ron Averes Updated [Location, Narrative]

Corrections or additions? ... Edit this accident description

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