ASN Wikibase Occurrence # 268886
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Date: | Tuesday 5 December 2000 |
Time: | 11:38 LT |
Type: | Mooney M20J |
Owner/operator: | |
Registration: | N4101H |
MSN: | 24-0616 |
Year of manufacture: | 1978 |
Total airframe hrs: | 3200 hours |
Engine model: | Lycoming IO-360 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | DANBURY, Connecticut -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | (DXR) |
Destination airport: | BEAUFORT , NC (MRH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane sat on the ramp for about 2 1/2 weeks with the fuel tanks half filled. Outside air temperature had dipped to 18 degrees Fahrenheit the previous night, and was still below freezing about 3 hours before the accident. Temperature at the time of the accident was 43 degrees Fahrenheit. The pilot did not check the fuel for water prior to the accident flight. After a normal start, run-up, and takeoff, the engine failed at 400 to 500 feet in the air, and the pilot made a forced landing. Evidence of water was subsequently found in a container that held fuel removed from the airplane.
Probable Cause: Water/ice in the fuel system and the pilot's inadequate preflight inspection.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC01LA052 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB NYC01LA052
Revision history:
Date/time | Contributor | Updates |
15-Oct-2021 14:08 |
ASN Update Bot |
Added |
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