ASN Wikibase Occurrence # 272443
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Date: | Saturday 18 July 2009 |
Time: | |
Type: | Beechcraft B36TC Bonanza |
Owner/operator: | |
Registration: | ZS-MPB |
MSN: | |
Fatalities: | Fatalities: / Occupants: |
Aircraft damage: | |
Category: | Accident |
Location: | 25 km west of Kenhardt in the Northern Cape -
South Africa
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Phase: | |
Nature: | |
Departure airport: | Stellenbosch aerodrome (FASH) in the Western Cape Province |
Destination airport: | Upington International Airport (FAUP) in the Northern Cape Province |
Investigating agency: | CAA S.A. |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was on a private VFR flight from Stellenbosch aerodrome (FASH) to Upington International Airport (FAUP) when he detected the smell of oil and smoke in the cockpit of the aircraft. The aircraft then suffered an uncontained engine failure. The pilot executed a forced landing on a gravel road. He was not injured in the accident. The aircraft suffered damage to the engine, undercarriage and propeller. The aircraft had undergone maintenance prior to the flight, to replace a worn starter clutch. A clip seal retainer was omitted during the installation of the starter clutch to the engine. The omission of the clip seal retainer caused the oil seal to become partially detached from its housing. This resulted in loss of engine oil during the flight, causing the engine to seize, resulting in an uncontained failure. The pilot decided to execute a forced landing on a gravel road. The undercarriage did not extend because the master switch had been switched off prior to the landing gear being extended. The aircraft landed on the gravel road with the landing gear retracted. The pilot was not injured in the accident sequence. The aircraft suffered damage to the undercarriage and the propeller in addition to the engine damage prior to landing. Probable Cause Probable cause The electrical master switch was disarmed during the uncontained engine failure in flight, and thereafter the emergency system was not utilised to lower the landing gear, resulting in a wheels-up landing. Contributory factor (1)The pilot's actions during the uncontained engine failure indicated that his knowledge and understanding of the aircraft's emergency systems and procedures were inadequate. (2) A clip seal retainer had been omitted during installation of the starter clutch to the engine, resulting in the seal becoming dislodged during flight.
Accident investigation:
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Investigating agency: | CAA S.A. |
Report number: | |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
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Sources:
S.A. CAA
Revision history:
Date/time | Contributor | Updates |
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