ASN Wikibase Occurrence # 27310
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Date: | Tuesday 24 September 1996 |
Time: | 10:15 LT |
Type: | de Havilland Canada DHC-2 Beaver |
Owner/operator: | U.s. Govt. Dept Of Interior |
Registration: | N67207 |
MSN: | 305 |
Year of manufacture: | 1951 |
Total airframe hrs: | 10869 hours |
Engine model: | P&W R-985 |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | King Salmon, AK -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | Brooks Camp, AK |
Destination airport: | (KAKN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot and three passengers were departing a remote lake in a float equipped airplane. The pilot positioned the hydraulic actuated flaps to 20 degrees. After takeoff, about 150 ft above the water, the pilot positioned the flap lever to the 'UP' position in preparation of pumping the flaps up, but said he did not move the pump handle. Turbulence was present during the takeoff, and during a left turn, the pilot encountered a severe gust at the time he positioned the flap lever. The airplane stalled in a left turn that steepened to almost a 90 degree bank. The airplane descended and the left wing contacted the surface of the lake. The left wing was torn off the fuselage, and the floats were crushed upward. Both flaps are activated by a common torque tube connected to a double-acting flap actuating cylinder. At the accident scene, the right wing flap and right aileron were observed to be extended to an intermediate position. The weather conditions included 20 kts of wind, turbulence, and rain. The pilot expressed a concern that the flaps may have retracted without being pumped to the up position. An examination of the flap system and the ratchet valve assembly was conducted after the airplane was recovered and the wings were removed. Leakage of hydraulic fluid and air was observed through the ratchet valve. Additional testing of the ratchet valve at an overhaul facility did not reveal any leakage.
Probable Cause: failure of the pilot to maintain sufficient airspeed during the initial climb after takeoff, which resulted in an inadvertent stall and collision with the terrain (water). Turbulence was a related factor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC96TA163 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB ANC96TA163
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
22-Oct-2009 22:28 |
DColclasure |
Updated |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
11-Oct-2017 17:57 |
TB |
Updated [Cn, Departure airport, Narrative] |
08-Apr-2024 18:52 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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