ASN Wikibase Occurrence # 274303
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Date: | Tuesday 18 January 2022 |
Time: | 11:00 |
Type: | Cessna 120 |
Owner/operator: | Private |
Registration: | N90129 |
MSN: | 9190 |
Year of manufacture: | 1946 |
Total airframe hrs: | 4733 hours |
Engine model: | Continental C-85-12F |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sylvania Airport (C89), Sturtevant, WI -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Sylvania Airport, WI (C89) |
Destination airport: | East Troy Airport, WI (57C) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On January 18, 2022, about 1100 central standard time, a Cessna 120 airplane, N90129, was substantially damaged when it was involved in an accident near Sturtevant, Wisconsin. The private pilot sustained serious injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
A review airport security camera footage showed the airplane was attempting to depart to the east. About a quarter way down the length of the runway after the beginning of the takeoff roll, the airplane departed the runway to the left (north). Airport security video footage showed the airplane travel over a flat grass field with the engine running. The footage did not show the airplane become airborne at any time, and the tailwheel appeared to remain on the ground during the runway excursion. The airplane came to rest after it impacted the cabin of an unoccupied, parked fuel truck. The pilot reported he recalled taxiing for takeoff and applying engine power for the takeoff; however, he was unable to recall any additional events.
Postaccident examination of the airframe revealed no mechanical anomalies.
The postaccident emergency care did not identify any medical conditions the pilot had that might have contributed to the accident. The pilot's pre-accident use of atorvastatin, famotidine, and fexofenadine, all non-impairing medications identified by toxicology testing of the pilot's samples, also did not contribute to the circumstances of this accident.
It is likely a loss of control occurred during the takeoff, which resulted in a runway excursion and a collision with an object. Based on the available evidence, the reason for the loss of control could not be determined.
Probable Cause: The pilot's loss of directional control during the takeoff for reasons that could not be determined based on the available evidence, which resulted in a runway excursion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN22LA103 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB CEN22LA103
https://data.ntsb.gov/Docket?ProjectID=104536 FAA register:
https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=90129 Location
Images:
Revision history:
Date/time | Contributor | Updates |
18-Jan-2022 20:56 |
Captain Adam |
Added |
21-Jan-2022 01:41 |
johnwg |
Updated [Time, Departure airport, Destination airport, Source, Damage, Narrative] |
11-Jun-2023 08:10 |
ASN Update Bot |
Updated [[Time, Departure airport, Destination airport, Source, Damage, Narrative]] |
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