ASN Wikibase Occurrence # 274965
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 31 January 2022 |
Time: | 12:53 |
Type: | Cessna 195 |
Owner/operator: | Private |
Registration: | N597K |
MSN: | 7403 |
Year of manufacture: | 1949 |
Total airframe hrs: | 2673 hours |
Engine model: | Jacobs R755-B2 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Palm Coast, FL -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Spruce Creek Airport, FL (7FL6) |
Destination airport: | Palm Coast-Flagler County Airport, FL (KFIN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On January 31, 2022, about 1253 eastern standard time, a Cessna 195 Airplane, N597K, was substantially damaged when it was involved in an accident near Palm Coast, Florida. The pilot and pilot-rated passenger received minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
The pilot and the pilot-rated passenger departed their home airport to fly to a nearby airport about 20 minutes away. The pilot stated that he did not add any fuel to the airplane before the flight, as he thought he had enough fuel for the intended 20-minute flight. He reported that before takeoff everything was normal. He took off, and upon reaching 1,000 feet above mean sea level (msl), he configured the airplane for cruise. The airplane was operating normally when, about 5 miles from the destination airport, the engine lost power. The propeller continued to windmill, but it produced no power. He attempted to restart the engine without success. The pilot declared an emergency and informed air traffic control (ATC) that he would be landing on an interstate. During the forced landing, the airplane's right wing contacted a truck, and the airplane came to rest inverted off the right side of the interstate, incurring substantial damage. The passenger said that he was worried about fire, and immediately tried to get out of the airplane. Once the passenger was out of the airplane, though, he did not see any fire or smoke, and there was no smell of fuel.
During the wreckage recovery, there was also no smell of fuel at the accident scene, with the exception of a slight smell of fuel near the engine. Additionally, no fuel could be recovered from the airplane. The postaccident examination of the airplane and engine also revealed no evidence of any preimpact mechanical malfunctions or failures that would have precluded normal operation. Additionally, the fuel strainer and the carburetor float chamber were absent of fuel.
An engine monitor was installed on the airplane that recorded exhaust gas temperature (EGT), cylinder head temperature (CHT), and shock cooling rate. During the accident flight, it recorded a rapid decrease in EGT, a rapid increase in shock cooling, and a rapid decrease in CHT, all of which in combination were indications that were consistent with of a loss of fuel flow.
The passenger stated that after the accident the pilot was “absolutely confident' that he had enough fuel for the 20-minute flight, and that the pilot said his fuel totalizer showed 23 gallons. However, the airplane's fuel totalizer required that a known fuel quantity be programmed at the beginning of the flight. If an accurate quantity had not been entered by the pilot at some previous point, the information indicated by the fuel totalizer would not have been correct.
Based on the available information, it is likely that the loss of power was due to the fuel system containing little or no usable fuel, as no fire occurred during the impact sequence, the passenger did not observe fire or smell fuel when he egressed, no fuel was able to be recovered on-scene during the wreckage recovery, the fuel strainer and carburetor float chamber were absent of fuel, and examination of the engine revealed no evidence of any preimpact failures or malfunctions which would have precluded normal operation. The circumstances of the accident were consistent with a total loss of engine power due to fuel exhaustion, which resulted from the pilot's inadequate fuel planning and preflight inspection.
Probable Cause: The pilot's inadequate fuel planning and preflight inspection, which resulted in a total loss of engine power due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA22LA112 |
Status: | Investigation completed |
Duration: | 1 year and 12 months |
Download report: | Final report |
|
Sources:
NTSB ERA22LA112
https://data.ntsb.gov/Docket?ProjectID=104580 https://registry.faa.gov/AircraftInquiry/Search/NNumberResult?nNumberTxt=597K https://flightaware.com/live/flight/N597K Location
Images:
Photo: NTSB
Media:
Revision history:
Date/time | Contributor | Updates |
31-Jan-2022 20:56 |
harro |
Added |
31-Jan-2022 20:57 |
harro |
Updated [Operator, Source, Embed code, Category] |
31-Jan-2022 20:57 |
harro |
Updated [Time] |
01-Feb-2022 08:35 |
retired George |
Updated [Source] |
01-Feb-2022 15:59 |
johnwg |
Updated [Time, Location, Nature, Source] |
02-Feb-2022 09:14 |
Captain Adam |
Updated [Location] |
04-Feb-2024 19:05 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Embed code, Narrative, Accident report] |
05-Feb-2024 21:38 |
Captain Adam |
Updated [Time, Operator, Location, Phase, Departure airport, Source, Embed code, Narrative, Photo] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation