ASN Wikibase Occurrence # 275467
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 8 February 2022 |
Time: | 09:45 LT |
Type: | Aeronca 11AC |
Owner/operator: | |
Registration: | N9500E |
MSN: | 11AC-1135 |
Year of manufacture: | 1946 |
Total airframe hrs: | 2174 hours |
Engine model: | Continental A-65-8 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Napa, CA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Davis-University Airport, CA (KEDU) |
Destination airport: | Santa Rosa-Sonoma County Airport, CA (STS/KSTS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was flying the airplane to an airport about 48 miles from the departure airport when, 30 minutes after departure while in cruise flight, the engine lost all power. The pilot then verified engine controls were at their correct positions and adjusted the carburetor heat setting. There was no change in engine power, so he made a mayday call and landed the airplane in an open field, during which the airplane sustained substantial damage to the lower fuselage.
A postaccident examination of the engine revealed that both magnetos produced a weak spark on all ignition leads when the propeller was rotated by hand. The left magneto was found to be in poor condition and did not function within the manufacturer's specifications. Internal examination of the left magneto revealed that the distributor axle bearing had failed, and the distributor gear was missing about half of its gear teeth. The right magneto was found in poor overall condition and was missing about 6 distributor gear teeth; however, it did function within the manufacturer's specifications. A review of maintenance records revealed no indication that the left and right magnetos were serviced, to include inspections or overhauls, since the engine's last overhaul 15 years (or about 400 hours) before the accident.
While the left magneto was not functioning within the manufacturers specifications, and the right magneto functioned within the manufacturers specifications, it would not result a total loss of engine power. The reason for the total loss of engine power could not be determined.
Probable Cause: The loss of engine power for undetermined reasons, which resulted in an off-airport landing on unimproved terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR22LA099 |
Status: | Investigation completed |
Duration: | 2 years 1 month |
Download report: | Final report |
|
Sources:
NTSB WPR22LA099
Location
Revision history:
Date/time | Contributor | Updates |
13-Feb-2022 12:12 |
Captain Adam |
Added |
04-Apr-2024 10:03 |
ASN Update Bot |
Updated [Time, Operator, Total occupants, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation