ASN Wikibase Occurrence # 278761
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Date: | Wednesday 19 May 2021 |
Time: | 11:00 LT |
Type: | Cessna T210N |
Owner/operator: | Keystone Aerial Surveys Inc |
Registration: | N7568N |
MSN: | 21063235 |
Year of manufacture: | 1979 |
Total airframe hrs: | 4070 hours |
Engine model: | Continental TSIO-520-R9B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bloomsburg, Pennsylvania -
United States of America
|
Phase: | Landing |
Nature: | Survey |
Departure airport: | Philadelphia-North Philadelphia Airport, PA (PNE/KPNE) |
Destination airport: | Philadelphia-North Philadelphia Airport, PA (PNE/KPNE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that during an aerial observation flight he finished the survey block and decided to land at an airport nearby to use the restroom and get fuel. He reported that he had never been to the airport, so he chose to enter the traffic pattern 'a little high†as he noticed terrain around the airport. On final approach, the pilot executed a forward slip maneuver to reduce 'excess airspeed and altitude†and once over the runway, he entered the landing flare, and the airplane floated down the runway about 500 ft. Subsequently, the airplane touched down nose first and entered a porpoise, which resulted in the collapse of the nose landing gear and a runway excursion through the end of the runway. The airplane sustained substantial damage to the fuselage and left wing.
The passenger on-board, who was the sensor operator, reported that while on short final approach, he observed the airspeed to be 125 knots, with a descent rate of 1,250 feet per minute, and the airplane subsequently touched down â€halfway down†the runway. He then described that the airplane began to porpoise, and the pilot retracted the landing gear and applied full power, however the airplane â€hit the ground†again and slid off the runway.
The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.
Probable Cause: The pilot's unstable approach and delayed go-around attempt, which resulted in a porpoised landing, a nose landing gear collapse, and runway excursion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA21LA268 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB ERA21LA268
History of this aircraft
Other occurrences involving this aircraft
12 May 1989 |
N7568N |
Huggs, Garriott, Ming |
0 |
Monterey, CA |
|
sub |
Location
Revision history:
Date/time | Contributor | Updates |
03-Jun-2022 19:45 |
ASN Update Bot |
Added |
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