ASN Wikibase Occurrence # 278954
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Date: | Thursday 2 May 2019 |
Time: | 17:02 LT |
Type: | Cirrus SR20 |
Owner/operator: | Arrive Aviation LLC |
Registration: | N8160C |
MSN: | 1381 |
Year of manufacture: | 2003 |
Total airframe hrs: | 2108 hours |
Engine model: | Continental IO-360-ES |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mineral Wells, Texas -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Fort Worth Meacham International Airport,TX (FTW/KFTW) |
Destination airport: | Weatherford-Parker County Airport, TX (WEA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was conducting a personal flight in the airport traffic pattern when he felt the airplane 'shudder†shortly before the turn onto the base leg for the runway. The pilot and passenger then saw the right aileron 'fluttering,†and the pilot immediately turned to intercept the final approach. The right aileron separated from the wing about 0.5 mile from the approach end of the runway. The pilot was able to maintain roll control of the airplane after the right aileron separated, and he completed an uneventful landing on the runway.
Examination of the airplane and the recovered right aileron revealed that the aileron's inboard hinge bolt was not threaded into its nut plate. The safety wire that normally secured the inboard hinge bolt was found fractured. The safety wire had been excessively twisted when the right aileron was installed; the excessive twisting led to the torsional overstress fracture of the safety wire during the accident flight. Additionally, the nut plate had significantly reduced thread-locking abilities that allowed the unsecured inboard hinge bolt to loosen; the right aileron separated from the wing when the inboard hinge bolt disengaged from the nut plate. Although the inboard hinge bolt assembly included a slightly longer bolt than specified and an additional small washer, these component discrepancies did not contribute to the aileron separation.
The airplane had accumulated about 733 flight hours during the more than 10 years since the right aileron was last removed and reinstalled during maintenance. The most recent maintenance performed on the airplane was an annual inspection completed about 15.2 flight hours before the accident. The mechanic who performed the last annual inspection observed safety wire installed on the aileron hinge bolts.
Probable Cause: The in-flight separation of the right aileron when the inboard hinge bolt disengaged from its nut plate due to excessively twisted safety wire, which resulted in a torsional overstress fracture that caused the inboard hinge bolt to become unsecured.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19LA133 |
Status: | Investigation completed |
Duration: | 2 years and 10 months |
Download report: | Final report |
|
Sources:
NTSB CEN19LA133
Location
Revision history:
Date/time | Contributor | Updates |
05-Jun-2022 13:11 |
ASN Update Bot |
Added |
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