Incident Boeing 767-332ER (WL) N181DN,
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ASN Wikibase Occurrence # 281440
 
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Date:Thursday 7 July 2022
Time:17:30 UTC
Type:Silhouette image of generic B763 model; specific model in this crash may look slightly different    
Boeing 767-332ER (WL)
Owner/operator:Delta Air Lines
Registration: N181DN
MSN: 25986/446
Year of manufacture:1992
Total airframe hrs:131342 hours
Engine model:P&W PW4000 SER
Fatalities:Fatalities: 0 / Occupants: 133
Aircraft damage: None
Category:Incident
Location:NE of Goose Bay, Canada -   Atlantic Ocean
Phase: En route
Nature:Passenger - Scheduled
Departure airport:Praha-Václav Havel Airport (PRG/LKPR)
Destination airport:New York-John F. Kennedy International Airport, NY (JFK/KJFK)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight crew of Delta Air Lines Flight 211reported that they experienced roll control difficulties after being informed of a water leak emanating from the two mid cabin lavatories while enroute from the Václav Havel Prague Airport (PRG), Prague, Czechia to the John F Kennedy International Airport (JFK), New York, New York.

The event flight was a Line Check flight flown by two complete crews, each consisting of a captain and a first officer (FO). The flight crew who was flying at the time of the event indicated that a flight attendant called and informed them of water leaking from the two mid cabin lavatories.

The flight crew who was not flying at the time confirmed that one lavatory was leaking water from under the lower right side of the toilet onto the floor; the water supply was subsequently shut off and the lavatory was locked to prevent further use. The other lavatory was leaking water from on top of the filter canister under the sink; the water supply to the sink was subsequently shut off and the lavatory was left open for toilet use only. The crew cleaned up as much excess water from the floor as possible.

The FO who was the pilot flying during the event stated that shortly after the water leak was reported, an AUTOPILOT caution message was displayed on the engine indicating and crew alerting system (EICAS) screen, along with an audible annunciation. The FO disengaged and reengaged the autopilot several times, however the caution messages, and audible indication persisted, and the aircraft made no lateral course corrections. The FO stated that he then disengaged the autopilot and attempted to make the course corrections manually; however, he was unable to move his control wheel to the left more than a couple of degrees of deflection and was thus unable to input the needed corrections. He then transferred control of the airplane to the captain, who confirmed the FO’s findings of minimal control to the left about the longitudinal axis of the airplane.

The FO stated that a “Jammed or Restricted Flight Controls” procedure was performed, and, in coordination with dispatch and maintenance control, it was determined that frozen water was a suspected cause due to the multiple water leaks. The flight crew declared an emergency and was given clearance to descend to 9,000 ft where the temperature was above freezing.

As the airplane descended through 12,000 ft, a minor “jolt” was felt by the flight crew. After this, the control wheel operated normally, and the flight continued to and landed safely at JFK. There were no injuries to the 233 passengers and crew onboard the airplane.

A review of flight data by Boeing revealed evidence of a temporary restriction in the lateral control system, starting shortly before the initial disconnect of the center autopilot. The evidence of a restriction was apparent in both automatic and manual flight and continued until shortly after the descent began from flight level (FL) 360. During the period of restricted movement, the captain’s control wheel showed a restriction at approximately 7 degrees of deflection to the left.

Boeing indicated that the 767 lateral flight control system is designed to allow for the override of a restriction in either the captain’s or FO’s flight controls by applying a breakout force to the control wheel on the opposite side. Boeing’s review of the flight data did not find evidence that the airplane lost the ability for an override to take place. The FO’s control wheel position, and control wheel forces for both wheels, is not recorded on the flight data recorder (FDR). The FDR data and statements by the flight crew on the incident flight were inconclusive about the total force input into the flight control system during the event.

According to Delta Air Lines, during corrective action after the subject event, the forward and aft lavatory drain mast heater circuit breakers (CBs), located in the electronic equipment bay, were found open. Although there were no current or previous maintenance write-ups on these heaters, Delta removed and replaced them as a precaution. Subsequent testing found the heater elements for the forward drain mast functioned normally.

Delta Air Lines reported that before the subject event, this airplane was out of service for maintenance which required pulling the forward and aft lavatory drain mast heater CB’s. It is possible that these CBs were inadvertently left open when the airplane was returned to service on June 23, 2022.

Due to the open drain mast heater CBs, it is likely that ice formed in the forward drain mast, allowing drain water from all equipment routed to the forward drain mast to back up in the lines until it leaked outside of the drain system plumbing. The water likely traveled into and drained through the canted pressure bulkhead in the vicinity of aileron control system components located within the main landing gear wheel well. The water likely froze on one or more of the components which led to the pilots’ limited control of the ailerons. Boeing could not identify a location in the roll flight control system where ice formation could restrict both the left and right ailerons if the control wheel breakout was activated.

Probable Cause: The failure of maintenance personnel to close the drain mast heater circuit breakers which resulted in the formation of ice in the forward drain mast, an improper flow of wastewater into the main landing gear wheel well, and the formation of ice on one or more aileron system components.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DCA22LA179
Status: Investigation completed
Duration: 9 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
12-Aug-2022 18:18 harro Added

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