ASN Wikibase Occurrence # 284040
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 25 November 2007 |
Time: | 16:00 LT |
Type: | Lake LA-4-200 Buccaneer |
Owner/operator: | Private |
Registration: | N1055L |
MSN: | 648 |
Total airframe hrs: | 1435 hours |
Engine model: | Lycoming IO-360-A1B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Jacksonville, Florida -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Jacksonville-Cecil Airport, FL (VQQ/KVQQ) |
Destination airport: | Jacksonville Executive at Craig Airport, FL (CRG/KCRG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, the "flight departed VFR from KVQQ at 15:55 for flight to KCRG. After departing Class D airspace to [the] southeast the pilot descended over the St. Johns River approximately 1/2 na[utical] mile offshore to practice reading wind direction from [the] water surface. The winds were very light and [the] water surface [was] mostly glassy. [The] pilot descended from about 2,500 ft. to approximately 100 ft. above [the] water and made several circles to [the] right to view [the] water. [The] pilot then leveled [the] wings and the [air]plane then bounced unexpectedly on the water and made about two more bounces before spinning to the left. [The] aircraft came to a stop and [the] pilot and passenger exited [the] cockpit onto [the] wing and were picked up by a passing motor boat. The plane sank after about 3 minutes." The pilot further stated that "this accident was caused by a glassy water condition and the pilot loosing depth perception. [The] pilot had no intention of landing and was practicing reading water for wind direction where wind was very light or none at all. [The] pilot had been endorsed on September 11, 2007 for SES [Single Engine Sea] practical testing but had not taken [the] check ride."
Probable Cause: The pilot's failure to maintain altitude while maneuvering over water. Contributing to the accident was glassy water conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA08CA019 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB MIA08CA019
Revision history:
Date/time | Contributor | Updates |
30-Sep-2022 06:54 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation