Accident Piper PA-24-250 N7961P,
ASN logo
ASN Wikibase Occurrence # 284233
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Tuesday 25 September 2007
Time:08:25 LT
Type:Silhouette image of generic PA24 model; specific model in this crash may look slightly different    
Piper PA-24-250
Owner/operator:Private
Registration: N7961P
MSN: 24-3198
Year of manufacture:1962
Total airframe hrs:3363 hours
Engine model:Lycoming O-540-A1D5
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Wimauma, Florida -   United States of America
Phase: Unknown
Nature:Test
Departure airport:Wimauma, FL (FD77)
Destination airport:Wimauma, FL (FD77)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot/mechanic reported that the engine oil quantity checked satisfactory during his preflight inspection. There were no discrepancies reported during his engine run-up which lasted 6 minutes, and included cycling the propeller "numerous times." The oil pressure and engine rpm checked good during the takeoff roll for the intended flight once around the traffic pattern. After gear retraction when the flight was past the departure end of the runway, the pilot noticed the oil pressure was zero. He entered a left downwind for runway 09, reduced throttle, then elected to perform a precautionary landing on runway 27. He made a left descending turn and while on a close-in left base for runway 27 while flying at 200 feet, he lowered the landing gear. He then added power but the engine did not respond. The pilot reported that the airplane stalled, then impacted the ground and slid to a stop. Postaccident examination of the airplane revealed no oil leakage from the engine which contained the same quantity of oil reported by the pilot during his preflight inspection. Additionally, the oil pressure gauge was tested using air pressure and found to operate. Examination of the engine revealed no evidence of preimpact failure or malfunction.

Probable Cause: The failure of the pilot to maintain airspeed while maneuvering for a precautionary landing following a reported loss of engine power for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA07LA157
Status: Investigation completed
Duration: 2 months
Download report: Final report

Sources:

NTSB MIA07LA157

Revision history:

Date/timeContributorUpdates
30-Sep-2022 13:44 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org