ASN Wikibase Occurrence # 284271
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 15 September 2007 |
Time: | 09:50 LT |
Type: | Beechcraft C90 |
Owner/operator: | N515KJ Aviation LLC |
Registration: | N515KJ |
MSN: | LJ-566 |
Year of manufacture: | 1972 |
Total airframe hrs: | 9031 hours |
Engine model: | Pratt & Whitney PT6A-20 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bloomingdale, Georgia -
United States of America
|
Phase: | Unknown |
Nature: | Ferry/positioning |
Departure airport: | Blairsville, GA (46A) |
Destination airport: | Savannah/Hilton Head International Airport, GA (SAV/KSAV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot said that he started the accident flight with 500 pounds of fuel, which he thought was sufficient for the flight. Approximately 12 miles from the destination airport both engines lost power. The pilot was vectored to a turf strip 2,700 feet long. He spotted the airport through breaks in the cloud layer and landed on the wet grass. The airplane overran the runway and impacted trees. The pilot stated that he determined the fuel quantity by referring to the fuel quantity gauges, and that the right fuel quantity indicator "consistently reads two hundred pounds less than the left" fuel quantity indicator. Postcrash examination of the airplane showed that it contained no usable fuel and there was no evidence of in-flight or postaccident fuel leakage from the airplane. No evidence of precrash failure of the aircraft fuel system or engines was found.
Probable Cause: A loss of engine power due to fuel exhaustion as a result of the pilot's improper preflight planning and preparation. Contributing to the accident was the pilot's reliance on inaccurate fuel gauges.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC07LA245 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB NYC07LA245
Revision history:
Date/time | Contributor | Updates |
30-Sep-2022 14:12 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation