ASN Wikibase Occurrence # 284349
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 31 August 2007 |
Time: | 15:45 LT |
Type: | Mooney M20K |
Owner/operator: | Hot Wings Aviation LLC |
Registration: | N231BQ |
MSN: | 25-0119 |
Year of manufacture: | 1979 |
Total airframe hrs: | 3280 hours |
Engine model: | Teledyne Continental TSIO-360 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fort Wayne, Indiana -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Auburn-De Kalb County Airport, IN (KGWB) |
Destination airport: | Indianapolis Metropolitan Airport, IN (KUMP) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane had just leveled off at 6500 feet, after departure, when the engine vibrated and lost full power. During an attempted return to the departure airport, the pilot realized that he could not make any runway and chose to make a forced landing into a corn field. The airplane was substantially damaged during the forced landing. Postaccident disassembly of the engine disclosed that the number two connecting rod had separated from the crankshaft; one of the connecting rod bolts had sheared. Inspection of the fracture surface of this connecting rod bolt disclosed there were signature marks of metal fatigue across the bolt shear face that had initiated at the surface of the bolt. The number two cylinder had been replaced about 8 hours prior to the accident; however, the connecting rod had not been removed from the crankshaft during the cylinder replacement.
Probable Cause: A total loss of engine power due to the fatigue failure of one of the number two cylinder connecting rod bolts.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI07LA287 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB CHI07LA287
Revision history:
Date/time | Contributor | Updates |
30-Sep-2022 15:26 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation