ASN Wikibase Occurrence # 284353
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 31 August 2007 |
Time: | 11:52 LT |
Type: | Beechcraft 35-B33 |
Owner/operator: | Private |
Registration: | N2133B |
MSN: | CD-563 |
Total airframe hrs: | 3604 hours |
Engine model: | Teledyne Continental IO-470-N |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tucumcari, New Mexico -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Tucumcari Airport, NM (TCC/KTCC) |
Destination airport: | Muskogee-Davis Field, OK (KMKO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Prior to departure, the airplane's fuel tanks were topped off with fuel, and the pilot "thought he adjusted his mixture control." The pilot reported that during the takeoff, he noticed no problems. During the gear retraction, the engine started to "act up." The pilot stated that the "act up" was not a sputtering or unusual noise, but that "the engine wasn't making the power that [I] expected." The pilot adjusted the mixture control to different lean and rich positions, with no change to engine power noted. The pilot then attempted a forced landing to a nearby interstate highway; however due to vehicle traffic, the pilot executed a forced landing to a field. Subsequently, the airplane touched down in a field with the landing gear retracted approximately 1 1/2 miles south of airport. Examination of the airplane revealed the right side of the fuselage was crushed upward and aft, and the right wing was bent. The propeller assembly and crankshaft propeller flange were separated from the crankshaft. The engine had accumulated 250 hours since major overhaul. Examination of the engine revealed mechanical continuity throughout the engine when the crankshaft was manually rotated. Continuity was established for the airframe and engine fuel system. The magnetos and wire harnesses were functionally tested and no anomalies were noted. Continuity was established from the cockpit to the throttle assembly, propeller governor, and mixture control. No anomalies were noted that would have precluded normal engine operation prior to impact.
Probable Cause: the pilot's failure to properly set the mixture prior to departing in high density altitude conditions, which resulted in a partial loss of engine power, and degraded climb capability.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN07LA150 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB DEN07LA150
Revision history:
Date/time | Contributor | Updates |
30-Sep-2022 15:26 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation