Accident Beechcraft 35-B33 N2133B,
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ASN Wikibase Occurrence # 284353
 
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Date:Friday 31 August 2007
Time:11:52 LT
Type:Silhouette image of generic BE33 model; specific model in this crash may look slightly different    
Beechcraft 35-B33
Owner/operator:Private
Registration: N2133B
MSN: CD-563
Total airframe hrs:3604 hours
Engine model:Teledyne Continental IO-470-N
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Tucumcari, New Mexico -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Tucumcari Airport, NM (TCC/KTCC)
Destination airport:Muskogee-Davis Field, OK (KMKO)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Prior to departure, the airplane's fuel tanks were topped off with fuel, and the pilot "thought he adjusted his mixture control." The pilot reported that during the takeoff, he noticed no problems. During the gear retraction, the engine started to "act up." The pilot stated that the "act up" was not a sputtering or unusual noise, but that "the engine wasn't making the power that [I] expected." The pilot adjusted the mixture control to different lean and rich positions, with no change to engine power noted. The pilot then attempted a forced landing to a nearby interstate highway; however due to vehicle traffic, the pilot executed a forced landing to a field. Subsequently, the airplane touched down in a field with the landing gear retracted approximately 1 1/2 miles south of airport. Examination of the airplane revealed the right side of the fuselage was crushed upward and aft, and the right wing was bent. The propeller assembly and crankshaft propeller flange were separated from the crankshaft. The engine had accumulated 250 hours since major overhaul. Examination of the engine revealed mechanical continuity throughout the engine when the crankshaft was manually rotated. Continuity was established for the airframe and engine fuel system. The magnetos and wire harnesses were functionally tested and no anomalies were noted. Continuity was established from the cockpit to the throttle assembly, propeller governor, and mixture control. No anomalies were noted that would have precluded normal engine operation prior to impact.

Probable Cause: the pilot's failure to properly set the mixture prior to departing in high density altitude conditions, which resulted in a partial loss of engine power, and degraded climb capability.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN07LA150
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB DEN07LA150

Revision history:

Date/timeContributorUpdates
30-Sep-2022 15:26 ASN Update Bot Added

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